CMS LEWA LDE1/M500 CO 2 pumps N° 574851-011.001 N° 574851-011.002.

Slides:



Advertisements
Similar presentations
Training Presentation
Advertisements

CHAPTER 45 Engine Lubrication.
USER MAINTENANCE.
“The Strength of Experience”
Brio 2000 / Brio 2000-M E-Learning Service Manual Rev. 0.0.
Servicing Welch DRYFAST ULTRA Pump Models 2032
What is a fastener? A device to locate or hold parts
Mechanical Integrity of Tubing
Metering Pump Spare Parts Replacement. Pump Components (Metering Pump) Pumps are supplied with a 120VAC or 240VAC power cord. Use care to ensure pump.
The pumps should be tightened about once a month. If a new pump is installed, the pump should be initially tightened and then re-torqued one week later.
ATLIER FRANCOIS (COMPRESSOR). MAINTENANCE AND CHECKS DAILY CHECKS DAILY CHECKS INSPECT AND NOTE THE OIL LEVEL AND ALL THE PRESSURE AND TEMPERATURE LEVELS(FILLL.
Morgan City Rentals Diesel Jet Pump 6 x 6 Peerless Safe Operating Practices and Procedures.
1B-1 Fire Engine Maintenance Unit 1B – Pump Inspections and Maintenance.
© 2012 Delmar, Cengage Learning Ordering Parts, Short and Long Blocks, and Engine Assembly Chapter 55.
COMMERCIAL REFRIGERATION
Section 5: Commercial Refrigeration
Diesel Generator Reliability: Lessons Learned from Storms
2012 JANUARY Sun Mon Tue Wed Thu Fri Sat
MOM Report Paul Soler MICE Operations Manager University of Glasgow MICO April 12, 2010.
IR2 and IR4 Summary PEP-II meeting Jan. 23, 2006 M. Sullivan.
Step 1 Park vehicle on a level surface then engage the parking brake and turn off engine. If you cannot comfortably get under the car, raise the front.
Feedwater Systems Reliability Users Group Annual Meeting January 20-23, 2014 Feedwater Pump Thrust Bearing Failure Presented By: Kurt J. Weis Rotating.
The Airtex Educational Partnership (AEP) was started several years ago by Airtex Automotive Division as a way to merge corporate automotive expertise with.
Hydraulics For The Long Term
© 2015 Cengage Learning. All Rights Reserved. May not be scanned, copied, duplicated, or posted to a publicly accessible website, in whole or in part.
© 2015 Cengage Learning. All Rights Reserved. May not be scanned, copied, duplicated, or posted to a publicly accessible website, in whole or in part.
Lockout Tagout Tryout (LOTO). The purpose of the Lockout Tagout Program is to protect you. Rain for Rent incidents include employees being sprayed with.
Engine Installation, Break-In, and In-Chassis Repairs
Griner Drilling Service
Staying in Compliance Dispensing Equipment Spill/Overfill Presented by B. J. Benton United Pump and Controls, Inc.
2013 NATEF Task Area A-2 Automatic Transmission A. General Transmission & Transaxle Diagnosis B. Transmission & Transaxle Maintenance & Adjustment.
1 Stony Brook Update Stretching your LEGS T.K. Hemmick for the tent crew.
ca Main Bullet #1 Main Bullet #2 Main Bullet #3 HXMA WIGGLER MAINTENANCE REVIEW Linda Lin June 2010.
1 A/C Pressure Test and Evacuation. 2 Leak Detection Leak detection must be done after every repair job. It must also be done anytime the appliance can.
Automotive Engines: Theory and Servicing, 6/e By James D Halderman © 2009 Pearson Education, Inc. Pearson Prentice Hall - Upper Saddle River, NJ
E8 / PPA Solar PV Design Implementation O&M Marshall Islands March 31-April 11, Preventive Maintenance.
DATE POWER 2 INCOME JANUARY 100member X 25.00P2, FEBRUARY 200member X 25.00P5, MARCH 400member X 25.00P10, APRIL 800member.
Raw Water System Flush By introducing fresh water into the cooling system, growth of sea life is reduced or eliminated keeping the raw water cooling pipes.
Copyright © 2003 General Motors Corporation.
2011 Calendar Important Dates/Events/Homework. SunSatFriThursWedTuesMon January
Oil Pressure Testing.
Overview of the main events related to TS equipment during 2007 Definition Number and category of the events Events and measures taken for each machine.
Staying in Compliance Dispensing Equipment Spill/Overfill Presented by Travis Benton United Pump and Controls, Inc.
17/6/2002Ivan Hruska,Francisca Calheiros,Bruno Allongue 1 Radiation test of PL500 in TCC2 Conclusion from last test in Louvain –All DCDC converters ran.
July 2007 SundayMondayTuesdayWednesdayThursdayFridaySaturday
CM2 Repair Status 8/13/2012 Tug Arkan 1. Latest Status After the warm end couplers were disassembled, it was decided to disassemble all the lower aluminum.
WELCOME TO HYDRAULIC-SAIVS. Bolting Tools Manufacturer Supplier Bolting tools are used to tighten or loosen the bolts or nuts and it also reduces the.
2015 Operations Stay Treat CHL2 4K Cold Box Modifications SC1 2K Cold Box CC4 Failure Helium and LN2 Losses Contamination Operations Stay Treat.
Fluid Mechanics for Chemical Engineers Arif Hussain (Lecturer)
University of Colorado – Boulder
MAGM 262 Hydraulic Seals Mr. Conrado.
Laser Monitoring System On behalf of the Caltech group
Forum on Tracking Detector Mechanics - Bonn, May 2016
Hongyu Bai LCLS-II 2 K Cold Box FDR March 9, 2017
Student CD for Commercial Refrigeration for A/C Technicians Chapter 12 Ice Machines.
What are the Parts Need to Replace For Resolving Transmission Fluid Leaks.
ITEMS TO CHECK ON Running Pumps
SB Packing Automatic Downpuller Power Unit
IBBelle: Status Commissioning at MPP Transport to KEK
CHAPTER 45 Engine Lubrication.
Year 2 Autumn Term Week 12 Lesson 1
2300 (11PM) September 21 Blue line is meridian..
Q1 External environment
Hydraulic Power System Accumulators, Actuators, Seals
Year 2 Autumn Term Week 12 Lesson 1
Philadelphia Scientific
Automatic Transmission/ Transaxle In-Vehicle Service
2015 January February March April May June July August September
Chapter 7: Classroom and shop manuals
Presentation transcript:

CMS LEWA LDE1/M500 CO 2 pumps N° N°

Order LEWA offer N°SLL from the 04/12/2013 DAI N° Created on the 13/12/2013 by Andrea d’Auria Order N°CA (1) sent to LEWA on the 16/12/2013 Pumps received at CERN on the 02/05/2014 and 13/05/2014

LEWA Pump N° Hydraulic oil leak history 20/04/2015 – 30/03/2016

Suspected gaskets Oil droplets Bolts that we have tried to tighten more but didn’t move… April 2015 First hydraulic oil leak detected in April 2015, after few hours of operations Mail sent to LEWA on the 20/04/2015

June 2015 First intervention of a LEWA technician on the 18/06/2015: Disassembly of the pump head and replacement of the damaged piston seal Problems during intervention: ◦Gear box oil in hydraulic circuit ◦Seal installed in wrong position JÉRÔME DAGUIN - EP/DT/FS

August 2015 Second intervention of a LEWA technician on the 05/08/2015: Disassembly of the pump head and replacement of the damaged piston seal Same intervention as on the 18/06/2015 Problems during intervention: ◦Hydraulic oil spilled on the floor Leak still present after few hours of operations… Mail sent to LEWA on the 07/09/ JÉRÔME DAGUIN - EP/DT/FS 6

September 2015 Third intervention of a LEWA technician on the 16/09/2015: Disassembly of the pump head and replacement of the damaged piston seal Scratch spotted on the piston. Polished with sand-paper Leak still present after few hours of operations… Mail sent to LEWA on the 25/09/ JÉRÔME DAGUIN - EP/DT/FS 7 Scratch on the piston Damaged seal Polished piston

December 2015 Forth intervention of a LEWA technician on the 04/12/2015: Disassembly of the pump head and replacement of the damaged piston and piston seal JÉRÔME DAGUIN - EP/DT/FS 8 Oil in the small reservoir

March 2016 After the intervention of the 04/12/2015, the pump was running with no leaks until the 14/12/2015 when it was stopped because of winter shutdown maintenance. Pump restarted on the 14/03/2016 and ran continuously until the 29/03/2016 On the 28/03/2016 around 17h00 the flow delivered by the pump (blue line) and the discharge pressure (yellow line) started to decrease with no apparent reason. Nothing was changed on the system at this time A visit on site on the 29/03/2016 revealed a new oil leak coming from the junction in between the head and the pipe connecting to the remote head The pump was stopped on the 29/03/2016 around 11:00. After consultation with LEWA technician all bolts were re- tightened and operation restarted… JÉRÔME DAGUIN - EP/DT/FS 9 Oil leak location Suction temperature Suction Pressure Mass flow Pump speed Discharge pressure

LEWA Pump N° Membrane spikes history 02/06/2015 – 30/03/2016

June 2015 First pressure spike in between the membrane spotted on the 02/06/2015 After discussion on the phone with LEWA, we inspected the head to check the presence of oil in between the two membranes (report from the 03/06/2015). No oil was found. On that date the head was found not properly tightened (4 out of 6 bolts not at the nominal 85 Nm torque) JÉRÔME DAGUIN - EP/DT/FS 11

November 2015 Pressure spikes reappeared in November and became problematic (pressure stayed high in between the two membranes) after 30/11/2015 Mail sent to LEWA on the 01/12/ JÉRÔME DAGUIN - EP/DT/FS 12 18/11/ /11/ /11/2015

December 2015 Operation not possible after the 01/12/2015: pressure in between the membranes rises after few minutes of operations… Mail sent to LEWA on the 02/12/ JÉRÔME DAGUIN - EP/DT/FS 13

December 2015 On the 04/12/2015, a technician from LEWA came to work on the other pump Describing our problem on this pump, he decided to replace the membrane (using our spare kit) During the intervention the ring that holds the membrane was found damaged Since no spare part was available on that day it was decided to reassemble the membrane with that ring and to change it in a later stage when available from the factory No pressure spikes were observed since the membrane replacement The pump was running from 04/12/2015 until 14/12/2015 and is now back in operations since 14/03/2016 On the 29/03/2016 we inspected the pump head (at the same time we inspected the other pump) and found some oil drops at the bottom of the head and few cm 3 in the bucket placed under the head This pump however does not show any signs of performances degradation and is still running up to now JÉRÔME DAGUIN - EP/DT/FS 14 Damaged membrane ring