Universitat de Barcelona Institut de Ciències del Cosmos ICC-UB

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Presentation transcript:

Universitat de Barcelona Institut de Ciències del Cosmos ICC-UB Progress on ICECAL chip test Upgrade of the front end electronics of the LHCb calorimeter D. Gascón, E. Picatoste, A. Sanuy, Universitat de Barcelona Institut de Ciències del Cosmos ICC-UB Calorimeter upgrade meeting – CERN – February 11th 2011

Key tests on the first prototype Test set-up Offset Noise Outline Introduction Key tests on the first prototype Test set-up Offset Noise Input impedance Linearity Flatness: jitter of clock vs input signal Characterization of preamp Summary & news LHCb Upgrade

ECAL analogue FE IC: channel architecture Introduction ECAL analogue FE IC: channel architecture Switched integrator Track and Hold First Prototype LHCb Upgrade

ICECAL chip Introduction Current preamp Integrators LHCb Upgrade SiGe BiCMOS 0.35um AMS 2 mm2 Received: October 2010 SiGe BiCMOS 0.35um AMS 2 mm2 Submitted: June 7th 2010 Current preamp Integrators LHCb Upgrade

Introduction: Current mode preamplifier Pros: “Natural” current processing Lower supply voltage All low impedance nodes: Pickup rejection No external components No extra pad Cons: Trade-off in current mirrors: linearity vs bandwidth Low voltage Only 1 Vbe for the super common base input stage Better in terms of ESD: No input pad connected to any transistor gate or base Inner loop: lower input impedance Outer loop: control input impedance LHCb Upgrade

Introduction: Integrator Switched integrator architecture FDOA specifications Parameter Value Gain bandwidth 500 MHz Phase margin > 65º Slew rate > 2 V/μs VCM 1.65 V FDOA CMOS switches LHCb Upgrade

Introduction: FDOA design Fully differential Operational Amplifier Common Mode Feedback NPN CE amp Folded cascode RDegenertion Pole compensation LHCb Upgrade

Key tests on the first prototype The purpose of this prototype is to test key points of a novel circuit idea: Input impedance control by current feedback Low noise performance Dynamic range: Linearity Also to test critical aspects of a switched solution: Offset between subchannels Noise “Flatness” of the integrator output Effect of jitter on clock versus signal Finally, the two key building blocks are prototyped separately in order to be characterized: Current preamplifier Fully differential OpAmp LHCb Upgrade

emulate clipping impedance Test set-up 50Ω || 50Ω = 25Ω ⇨ emulate clipping impedance Tektronix TDS7154B Oscilloscope: BW = 1.7 GHz 20 GS/s 8 bit Tektronix AWG2021 Waveform Generator: 250 MS/s 12 bit Differential probe: BW = 400 MHz Cin = 1 pF LHCb Upgrade

Test set-up Integrator clock signals generated with comparator Input circuit with AC coupling and Rpar Outputs are measured at ASIC outputs and after x10 amplification LHCb Upgrade

Test set-up LHCb Upgrade

Offset Offset measurement: Preamp current offset is integrated V at cycle end Preamp current offset is integrated => Offset at output 2 ns V offset LHCb Upgrade

Offset 5 % of dynamics About 5 % of the full scale range (2 V) Slight asymmetry between subchanels (clock) 5 % of dynamics Subch Mean [mV] Std Dev 1 27 20 2 34 35 LHCb Upgrade

Offset With AC coupling between ICECAL and ADC what really matters is the difference between the offset of the 2 subchannels Well below the 5 % of the full scale range (2 V) 5 % of dynamics LHCb Upgrade

Noise after dynamic pedestal subtraction Noise: simulation Transient noise analysis σ = 0.377 μV Noise Sampling time t1 Sampling time t2 0.78 ADC counts Integrator 1 output Clock Noise after dynamic pedestal subtraction rms = 2.29·10-4 mV σ = 0.479 mV 0.98 ADC counts Correlated noise: distribution of V(t2) Uncorrelated noise: distributon of V(t1)- V(t2) LHCb Upgrade

Noise The noise: Generate a histogram of the voltage value by the end of the cycle. Gaussian fit => standard deviation Noise is dominated by the differential probe at the ASIC output => use an amplifier of gain 10. Pantallazo amb els histogrames que hem mesurat Explicacio de la mesura, amb ampli… LHCb Upgrade

Noise Average noise is about 1.8 ADC counts, higher than expected Histogram is not fully Gaussian: Noise pick-up: Depends on chip connection (socket) LHCb Upgrade

Noise Alternative method: acquire 100 waveforms and make histogram LHCb Upgrade

Noise Alternative method: acquire 100 waveforms and make histogram Study effect of correlated sampling CDS (dynamic pedestal subtraction) Typically noise improves after CDS CDS increases uncorrelated noise (HF) CDS attenuates LF noise That confirms the presence of pick-up noise After CDS noise is about 1.2 ADC counts (close to simulation:1 ADC count) LHCb Upgrade

Noise On very few cases noise after CDS is higher 1.1 ADC counts before CDS 1.2 ADC counts after CDS That means that pick up noise and the increase of uncorrelated noise by CDS are comparable LHCb Upgrade

Input impedance Waveform Generator Test Pulse Vs. Clipped Pulse Recordar diagrama de blocs del set-up: Explicar paper de Rpar (esquema de l’entrada) Mostrar i explicar el senyal d’entrada curta per mesurar les reflexions (mesura – csv) Fast pulse (no tail) to measure reflections LHCb Upgrade

Input impedance PCB input circuit: AC coupling Rpar: Zin a little higher than 50Ω Rp used to fine tune Zin Recordar diagrama de blocs del set-up: Explicar paper de Rpar (esquema de l’entrada) Mostrar i explicar el senyal d’entrada curta per mesurar les reflexions (mesura – csv) Rp LHCb Upgrade

Input impedance Waveform Generator Source signal IC input signal (PCB) sbch1 INT sbch2 LHCb Upgrade

Input impedance ICECAL OFF Large reflections Waveform Generator Source signal IC input signal (PCB) Large reflections sbch1 INT sbch2 LHCb Upgrade

Input impedance Reflection coefficients Source (AWG) IC input (PCB) Reflection Coefficients for source, IC input, and output signals. Refl. Coeff. = 1st pulse integral / 2nd pulse integral Out sbch1 Out sbch2 INT LHCb Upgrade

Input impedance Optimal Rp is between 360 and 390 ohm Dynamic variation of input impedance is << 1 % for full dynamic (50 pC) Measurement error for second reflection is quite high for low amplitudes Noise of the differential probe Rp = 360 Ohm Rp = 390 Ohm LHCb Upgrade

Input impedance (12 chip statistics: new!) Dispersion is low: < 0.5 % Only 5 chips have been measured Mean [%] Std Dev First 1,99 0,21 Second -1,75 0,43 Int output -0,82 0,11 Rp = 360 Ohm LHCb Upgrade

Linearity (12 chip statistics: new!) Dynamic range is ok (50 pC required) Rp (input impedance) affects the amount of charge sensed by the ASIC Rp 360 Ohm: negative reflection coefficient: lower amplitude @ ICECAL input Rp 390 Ohm: positive reflection coefficient: higher amplitude @ ICECAL input Rp = 390 Ohm Rp = 360 Ohm LHCb Upgrade

Linearity (12 chip statistics: new!) Slight sistematic difference between subchannels (clock) ? Rp = 390 Ohm Subch Mean [mV/pC] Std Dev 1 34,84 0,41 2 35,13 0,32 Rp = 360 Ohm LHCb Upgrade

Linearity (12 chip statistics: new!) Relative linearity error is below 1% for the full range (50 pC) Very difficult calibration of the measurement system: Scope vertical scale and attenuation of the probe Cross-check using calibrated attenuators Problems with very low amplitudes: see next slides Still well below 1 % of the Full Scale LHCb Upgrade

Linearity What happens at low amplitudes? Problem with AWG generator: Different signal delay as fucntion of the amplitude (advanced for low amp) Again, it can be bypassed using calibrated attenuators LHCb Upgrade

Linearity Adding some delay for low AWG amplitudes corrects the problem In that case, relative linearity error is well below 1 % even for low amplitudes LHCb Upgrade

Flatness at the integrator output Setup: Problem: Due to clock jitter, the signal at the output must be stable (<1%) for 4 ns. Input signal: AWG generated similar to clipped (see next slide) Method: Delay clock signal in 1ns increments Use LEMO cable (minimum number of cables, 0 to 3) Measure output signal and analyze CLOCK LHCb Upgrade

Flatness at the integrator output Waveform Generator signal vs. Measured clipped signal (Anatoli) LHCb Upgrade

Flatness at the integrator output The output variation is smaller than 1% for about 3 ns delay variation Consistent for different signal amplitudes Can be improved using a resistor in parallel to the integrator capacitor LHCb Upgrade

Current preamp (0T): first results (new!) We just started characterization Current preamp (0T) Input range of about 4 mA peak current 4 mA peak LHCb Upgrade 36

Summary and news Measurements of the input stage (preamp+integrator) are about finished Principle is ok Good results with 12 chips statistics Need to study the effect of bias (op. paint) variation Characterization of individual blocks has started Preamplifier: Linear input range is almost 4 mA peak current Could tolerate unclipped signal Additional gain trimming should be foreseen Fully differential amplifier: TbD Impact of the residual amplification in reset? To be tested Additional switches ? Not needed according simulations Few % error in the tail ?

Summary and news We are preparing a new set-up: AUTOMATIZED IN CAT Analog mezzanine including ICECAL+ADC (see Carlos talk) Calibrated and programmable attenuators (avoid generator “jitter” problem) 12 bit 500 MHz (3 GS/s) DAQ: Wavecatcher (advertisement for Dominique) Pulse reflectometry to measure input impedance USB -> we should integrat it in CAT (or maybe it is done…) LHCb Upgrade 38

New blocks To be tested in future runs: Prototyped in June AMS run: Low noise current amplifier: Basic schemes Integrator: High GBW fully differential OpAmp Could be used in other stages To be tested in future runs: Compensation of process variation of amplifier’s input impedance Track and hold (if needed) Analogue multiplexer ADC driver ADC needs to be characterized Common blocks: Clock generation Biasing (CMOS band gap already exists) Ok, but need to add som tuneability 39 39

Plans Plans for 2011 And for 2012, if everything is ok… Test and design until Q3 2011 There is no clear need of making more “partial” prototypes Submit a prototype with few complete channels in Q4 2011 Still possible to send a critical block in June 2011 if needed Goal of submitting a complete channel in Q4 2011 should be preserved And for 2012, if everything is ok… Test beam ? Mind we said that in December, before Chamonix… Radiation tests? Long term: technology obsolescence… AMS 0.35 um is a “mature” techno We asked to Europractice: 5 years are “guaranteed” Low volume productions are scheduled Production (engineering run) is safe But for desin (MPW runs) we should not relax 40 40