Iowa State University Design Presentation

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Presentation transcript:

Iowa State University Design Presentation 3/8/2018 Alec Ehlke, Charlie Bootsmiller, Joe Regan

Content Entry Description Timeline and Team Management Innovations Results

Entry Description 2014 Polaris 800 Indy SP 750cc Weber MPE Turbocharged 2 Chamber, Custom reactive muffler Three-way catalytic converter MS3 Pro Ultimate ECU [MegaSquirt]

Timeline and Team Management Timeline created at start of season Tasks organized by sub- system team 4 sub-system teams Improved Team’s ability to uphold specific deadlines At the beginning of the season, a timeline was created by the tech and project director in Teamweek. Once the timeline was created, the map was shared with the assorted team leaders, and their concerns were identified. Once all parties were in agreement, the timeline was solidified and teams were expected to meet their deadlines in order to stick to the pre-determined plan.

Innovations 2 - Stroke to 4 - Stroke engine swap Custom Exhaust 304 Stainless Steel Ceramic Foam insulation Three-way Catalyst 3D metal printed downpipe Standalone ECU Skid and Body Modifications

Baseline and Engine Selection 800 cc Liberty – 2 stroke E-score of 76 [2015 results] 80 dBA [Custom muffler] 150 Stock Hp 750 cc Weber MPE - 4 stroke E-score of 176 [RIT 2015] 77 dBA [Stock muffler] 120 Stock Hp Stock in the Indy chassis is a 2 stroke 800cc liberty engine. This engine was used in our 2016 competition, and was used as the baseline for testing in this year’s design. 80 dBA 193.7 E score BSFC : 43.06

Engine Mounts Engine mount prototyping Finite Element Analysis Load [S.F. of 2] Natural Frequency - 133.33 rad/sec Mode 1 Frequency - 493.66 rad/sec

Standalone ECU Hardware Software MS3 Pro Ultimate Converted stock harness Innovate ECF-1 Wideband O2 and ethanol sensor Software TunerStudio MS Custom fuel and ignition tables MegaLogViewer MS data logs chose the ms3 because we are inexperienced with tuning, and tunerstudio is easy to navigate.

Skid and Body Modifications Graphite Hyfaxes Catalyst and nose-cone vents Sound deadening material addition Trial Pulling Force (lbs) Old Polyethylene Hyfax New Graphite Hyfax 1 15 13 2 12 3 14 4 16 11 5 Graphite hyfaxes were tested to confirm that they will have a lower coefficient of friction, therefore providing less resistance against the track during operation. The hyfaxes were tested by pulling a skid on a sheet of aluminum with a standard spring force gage. A sheet of aluminum was used to simulate the clips of the track that the hyfaxes would run against. Vents were added into the plastic to better manage the elevated temps in the engine bay during operation. A vent was added on the exhaust side of the sled where the catalyst is located to provide a steady stream of cool air against the surface of the catalyst. A forward facing vent was also added to provide supplementary cooling to the radiator and intercooler stack up with the FST stock radiator fan. In order to see the results, the nose-cone was simulated in Ansys with a 45 mph/20.11 m/s air stream speed. Initially, the max speed seen in the nose-cone was 26.7 m/s. After the geometry of the nose-cone was changed, the max speed see was 60.3 m/s. With the addition of further data such as the inlet and outlet temps and flowrates of coolant, the team would be able to simulate the thermal effect of the vent on the intercooler and radiator stack up. Graphite Hyfax Testing Results Nose-cone vent Ansys Analysis

Skid and Body Modifications Here is our data from last year. We went with the ⅛” Linex because it had the highest reductions of Decibels. Here is further analysis of sound deadening with various materials including: Plastic, Raam Mating, and Linex.

Custom Exhaust ANSYS Simulation Exhaust Alignment   Operating Temperature °F (°C) Carbon Steel 900 (500) Aluminized Steel 1200 (650) 304 Stainless Steel 1400 (760) 420 Stainless Steel/Brz 1650 (900) Downpipe 3D Printed, 420 Stainless with Bronze Catalytic Converter Aristo Global 3-Way Catalyst Muffler Double Walled / Ceramic Fiber Shell 304 Stainless Tubing Fiberglass Exhaust Wrap Material properties ANSYS Simulation Our baseline readings for the stock exhaust are 77dba which is already a much better improvement over the stock 2 stroke Indy. Exhaust Alignment

Goals and Lessons Learned Continue to innovate through simulation software Give more time for Engine Calibration Further pursue 4 - stroke engines Proper catalyst insulation 3D printing as a low production alternative and prototyping option Electrical team organization Pursue more effective emissions testing

Questions?