Summary and update on HGC Entrance Window Design and Testing

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Presentation transcript:

Summary and update on HGC Entrance Window Design and Testing Garth Huber Today is Thanksgiving Day in Canada! Informal SoLID HGC Review, Jefferson Lab, October 8, 2018.

HGC Prototyping Update C$100k grants allow the U.Regina group to construct one SoLID HGC module for testing. Questions to be addressed: Enclosure deformation at 1.5 atm operating pressure (investigate design and metal alloy options). Performance of the O-ring seals against adjacent units. Performance of thin entrance window in terms of light and gas tightness (test several options). Conceptual design by Gary Swift, Duke U. FRN: SAPIN-2016-00031 2 2

HGC Thin Window Prototyping Testing Requirements: Safely hold 2x operating pressure for extended time periods Minimize bulge for clearance in SoLID Reproducible fabrication Two prototype window frames: Full size window testing at +1 atm Quarter-scale version testing at +4 atm Above: Full size test window Left: Quarter-scale test window frame

Ripped epoxy-reinforced Kevlar window, which failed at 60 psi. All Mylar-Kevlar Windows Failed ¼-Scale Window Pressure Tests For same window tension as full size window, the maximum pressure needs to be increased 4x. i.e. Small window @ 60 psi roughly equivalent to full size window @ 15 psi. Repeated mechanical failures of Kevlar window near maximum pressure, even after epoxy strengthening, lead us to explore alternatives. Ripped epoxy-reinforced Kevlar window, which failed at 60 psi. 4 4 4

Carbon-Fiber Shell + Mylar Inner Window ¼-Scale Window Pressure Tests Hard shell constructed with 3x Fiber-Glast carbon- fiber and epoxy. 13”x17” shell is molded with a 5cm bulge depth, approximately circular profile. 3mil Mylar inner window beneath shell is used to seal against O-ring. Kevlar from previous test placed on top as a safety measure, as protection against a catastrophic shell failure. Fabrication of Carbon Fiber Shell in Regina Completed shell showing formed 5 cm bulge

Small Carbon-Fiber Shell + Mylar Results Substantially less deflection above initial height than reinforced Kevlar window. Carbon-Fiber Shell is mechanically stable at 60 psi. Discover that window frame is too weak, leaking around bolts. Temporarily reduce leak using C-clamps around frame. Deflection vs Pressure. The Carbon-Fiber shell had an initial bulge height of 5cm. Carbon-Fiber Shell has the required strength. Shell was reused in subsequent tests before failing. Results suggest clamping wire is interfering with the O-ring, and/or other sealing problems. 6 6

Failure of too-flat Carbon-Fiber shell at 60 psi Further Small Carbon-Fiber Shell Testing With promising results for 5cm bulge Carbon-Fiber Shell, further modifications were made: Decreasing the depth of the shell resulted in catastrophic failure! Still experienced issues with leaking, but ready to move to full-size window tests. Several questions to be addressed: What is the optimal bolt/wire/ O-ring arrangement on frame? How thick does the frame need to be to ensure adequate clamping? How many layers of carbon-fiber are needed? Can fractures in the shell be repaired and operate normally? Failure of too-flat Carbon-Fiber shell at 60 psi 7 7

Full Size Carbon Fiber Shell + Mylar Liner Hard shell constructed with 3x Fiber-Glast carbon- fiber and epoxy. 3mil Mylar inner window beneath shell is used to seal against O-ring. Kevlar on top as a safety measure in case of catastrophic failure. Above: Test jig for full size window shell Left: Foam mold for full size window shell

Full Size Carbon Fiber Shell + Mylar Results Moderate success with full size 3xCF shell: Structurally stable at +1 atm Failure in pressure seal due to previously identified frame issues Alarming creaking noises from shell under stress while inflating Deflection only 2cm beyond constructed bulge at maximum pressure New test frame following recent modifications forthcoming Replacement of O-ring with gasket being considered

Heavy Stock Flat Carbon Fiber Shell Heavier stock carbon fiber fabric from Fiber Glast. Try flat window (no preformed bulge) to improve clearance and simplify fabrication. Flat window structurally stable at +4 atm where previous flat window (with lighter CF) failed. Significantly reduced creaking noises over previous tests. Maintaining pressure for over 6 months with only small pressure drop (possibly due to atmospheric pressure variations). Very promising results from the thicker Carbon Fiber. Waiting for completion of full size version with this technique.

Next Steps If test of flat full-scale CF window is successful, we expect to have arrived at the final thin window design solution. After your design review is completed and all changes are made by Gary Swift, we will shift effort to fabrication of the prototype vessel. The grants from CFI and Fedoruk required the HGC prototyping project to be completed by Dec 31, 2018. Current Account Balance: C$59,654.81 As the project scope has expanded since the original proposal, both agencies recently approved a 1 year extension. Planned Prototype Vessel Schedule: Bids on largest vessel parts by vendors completed by January, delivered to UofR campus by April. In parallel, UofR machine shop makes smaller parts not sent out to vendor. Assembly, and testing during assembly, in Summer, 2019. Testing likely to identify further changes that we could try to implement before end of 2019 (this is the point of prototyping). Once we are done our tests, we could ship the prototype to either Duke or JLab for additional studies (such as PMT mounting, mirror placement), if desired.