Weekly Progress Update 13 April 2018

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Presentation transcript:

Weekly Progress Update 13 April 2018 UIG Resolution Weekly Progress Update 13 April 2018

DM read rejection update Pot 1 Key messages Outstanding last week = 4 Closed this week = 2 0 meter points still impacting UIG (estimated consumption not accurate) Row Labels DMSP N/A SHIPPER MAM XOS Grand Total Assigned Closed 175 Fix in Progress 1 2 New Monitor Failed Total 177 Total number of meter point queries open Pot 2 Key messages Outstanding last week = 29 New Rejections identified = 0 Closed this week = 12 5 meter points still impacting UIG (estimated consumption not accurate) Row Labels DMSP N/A SHIPPER MAM XOS Grand Total Assigned 3 2 8 Closed 162 Fix in Progress 1 6 Fixed New Monitor Total 4 5 176 Total number of meter point queries open 17

DM Financial Adjustments Progress POT 1: 177 (0) Root Cause Fixed: 169 (0) No CA Required/ Closed: 88 (+4) CA Needed: 76 (-4) New/Valid Contact Submitted: 45 (-4) Invoiced: 16 (0) Not Required: 5 (0) Complete: 11 (0) Kwh: 111,788,618 (0) In Progress: 20 (-6) Under Review: 11 (-9) Issue With Adj: 9 (+3) Awaiting Billing: 9 (+2) To Be Billed: 8 (+2) -78,945,281 -(5,872,222) Held Pending Rec: 1 (0) Shipper Notification Received: 31 (0) No Contact: 22 (-3) Invalid Contact: CA Decision Pending: Root Cause Pending: 8 (0) Accurate as of 11.04.2018 Exposure: Retrospective CA not yet invoiced = 73 (-4) [Root Cause Pending] + [CA Decision Pending] + [CA Needed] – [Invoiced]

Invoiced Figures (CA Only) Deemed Not valid: 5 (0) Complete: 11 (0) Jan-18: 1 Kwh: 0 GRE (£): 0.00 Feb-18: 4 Kwh: 128,335,231 GRE (£): 1,788,429.70 Mar-18: 6 Kwh: -16,546,613 GRE (£): -145,611.57 Apr-18: Pending Kwh: tbc GRE (£): tbc Kwh value represents the primary debit/(credit) equal and opposite value feeds UIG Reconciliation Accurate as of 11.04.2018

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