Tom Peterson TESLA Technology Collaboration Meeting Feb 2019

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Tom Peterson TESLA Technology Collaboration Meeting Feb 2019
Presentation transcript:

Tom Peterson TESLA Technology Collaboration Meeting Feb 2019 Experience with cryogenics induced microphonics in an LCLS-II cryomodule Tom Peterson TESLA Technology Collaboration Meeting Feb 2019

LCLS-II microphonics was observed from several sources Thermo-acoustic oscillations in valves Gate valve supported from pipe, hard-connected to cavity 1 Cool-down valve leak bubbling into the helium vessel bath Focus on this latter Flow-induced microphonics, TTC, Feb 2019

Cryomodule flow scheme Peterson, Fast Cool-down, 28 Nov 2017

Upstream end showing capillary tubes for cool-down and warm-up LCLS-II Cryomodule, Peterson, 28 Sep 2015

pCM (Prototype CM) Cryogenics Distribution System Flow-induced microphonics, TTC, Feb 2019

Summary from my 31 Aug 2017 Weekly Report Microphonics in Fermilab CM F1.3-04. New microphonics appears to have been due to a cool-down valve leak sending a low flow rate of helium continuously into “line H”, the cool-down manifold and into the cavity helium vessels via the capillary tubes. Phase separation and/or temperature stratification of this low flow in line H likely sends warmer helium to cavities at the upstream (uphill) end, which is consistent with the observation of worse microphonics at the upstream end. Analysis confirms that low flow rates such as via a valve leak may send vapor all the way into the helium vessel, where collapsing bubbles could generate microphonics. Replacement of the cool-down valve stem fixed the microphonics problem in that F1.3-04 subsequently looked like F1.3-03. Flow-induced microphonics, TTC, Feb 2019

Cooldown Leakage Theory Leakage through the cooldown valve was verified by isolation of 2K supply upstream Gas flow through cooldown circuit caused unexpectedly narrow frequency lines which has been identified as streams of bubbles Gas flow as a cause was determined by large harmonics of these lines and complex spatial dependence upon perturbation as gas flow shifted around module Flow-induced microphonics, TTC, Feb 2019

Cryogenic Valve Plumbing – Cooldown Valve Leakage F1.3-04 presented with higher than expected microphonics, worsening as the cryomodule thermalized F1.3-07 showed same noise after 3rd temperature bump Both characterized by solidly low temperature cooldown line (2 K vs ~25 K), indicating active flow Noise was narrowband and showed complex spatial and spectral distribution in cryomodule Testing showed noise to be coherent bubbling due to cooldown valve leakage, explains noise on upstream cavities Swapping valve stem returned expected performance in both cases Tails seen in ‘post-swap’ data are likely due to continued thermalization of cryomodule after cooldown Additional QA check step now included to prevent valve leakage in the future Thermalized Detuning Post CD Stem Swap Flow-induced microphonics, TTC, Feb 2019

Microphonics and cryogenics data thanks to Acknowledgements Microphonics and cryogenics data thanks to Jeremiah Holzbauer Elvin Harms Cryogenic operators Many of these slides thanks to Jeremiah Flow-induced microphonics, TTC, Feb 2019

Backup Slides Flow-induced microphonics, TTC, Feb 2019

Cold mass cross section Bottom of the 2-phase pipe ID is 25 mm above the helium vessel ID top. Helium vessel is full to the top with any liquid in the 2-phase pipe. Center of the 2-phase pipe is 17 mm below the bottom of the HGRP. LCLS-II Cryomodule, Peterson, 28 Sep 2015

Sources of Microphonics – Measurements/Mitigations Helium Injection Flow-induced microphonics, TTC, Feb 2019

Mitigation Steps in Cryomodule Design – 2 Phase Injection Liquid level control was coupled to input flow rate and the amount of flash gas generated across JT valve Helium injection line impinged on liquid surface Flash gas from JT caused liquid dragging CM2 has baffles to protect liquid surface CM3 has tangential injection into cap to reduce velocity and allow phase separation in addition to baffles Should greatly reduce liquid dragging and improve liquid level stability, especially at high flow rates Fluid simulation gives good confidence in improved injection behavior CM2 CM3 Flow-induced microphonics, TTC, Feb 2019

High Heat Load F1.3-03 Testing Testing at high heat load (~125 W) shows very minor (~10%) degradation of detuning environment All cavities at gradient TAOs in CMTS-1 distribution system show no correlation with cavity detuning Gives confidence that flow dependent effects will have minimal impact on tunnel operation In tunnel operation will have lower inlet temperature (CMTS-1 has no JT heat exchanger), further lowering flow required in operation Similar behavior measured on F1.3-02 and F1.3-03 Low Flow Background High Flow – Unit Test Flow-induced microphonics, TTC, Feb 2019

J1.3-02 Data Was Taken With Valve Stems (Not Reversed Valves) Slides From T. Power (JLab) Flow-induced microphonics, TTC, Feb 2019

Need for Wipers F1.3-02 was tested with reversed valves but no wipers on JT and CD valve Increased valve bonnet temperature drop during cooldown Increase in unstable microphonics lines, to which Cavity 1 is especially sensitive 4K mode will be sensitive to increased heat load without wipers Flow-induced microphonics, TTC, Feb 2019

Brief Introduction to TAOs Thermoacoustic oscillations generally occur in long gas-filled tubes with a large temperature gradient. Acoustic modes couple to mass transport up and down column especially well when gas density is strongly tied to temperature. E.g. Warm gas from the top of a valve column moving to the cold bottom contracts, reducing pressure at warm region, driving the now cold gas back. Long valves and very low speed of sound in cold helium can easily give lowest acoustic modes at dangerous frequencies. The quarter-wave mode in a 1 meter valve filled with 5K helium has a resonant frequency of 130 [m/s] / 4 [m] = 32 [Hz]. These oscillations are generally important for the tremendous heat leaks they can represent, not microphonics. Flow-induced microphonics, TTC, Feb 2019

Thermo Acoustic Oscillation Dropping the helium supply pressure to below the critical point (18 psig) significantly improved microphonics levels. Although obviously not a realistic configuration, diagnostically, this was critical in our understanding of the detuning correlation with TAOs Wipers were installed on the valve stems JT first, but that alone was not enough Even with no flow, the cooldown valve still exhibited a TAO that disturbed the cavities Best performance was with wipers in all valve stems Temperature sensors on the valve bonnets still showed some TAO behavior, and microphonics wasn’t completely gone Flow-induced microphonics, TTC, Feb 2019

Static heat load significantly lower for lower JT inlet pressures Helium Consumption Static heat load significantly lower for lower JT inlet pressures Helium consumption falls by 60% Supercritical operation after fixes maintain a lower heat load (although not quite as low). Flow-induced microphonics, TTC, Feb 2019

High JT Flow Rates High JT flow rates (high JT inlet temperature leads to lots of flash gas) gives large flow velocities (up to 70% of the speed of sound!). JT injection hits directly on liquid surface (changed already in CM2). The flash gas must escape to chimney, and this will push liquid downstream. Remember that the upstream side is higher than the downstream side. Flow-induced microphonics, TTC, Feb 2019

Sloshing Mode in the 2-Phase Pipe Changing the flow from JT to Bypass meant significantly reduced gas flow in the 2-Phase pipe. When the JT is closed, the difference between Upstream and Downstream liquid level suddenly changes, rings down to a stable (hopefully level) point (40 second period). This couples liquid level and flow rate, complicating control. Flow-induced microphonics, TTC, Feb 2019

Cryogenic Distribution Improvements Needle Valve Volume Pressure Transducer Slide courtesy of Ben Hansen Flow-induced microphonics, TTC, Feb 2019