Sustained Treatment of AMD Containing Al and Fe 3+ with Limestone Aggregate Neil Wolfe and Robert Hedin Hedin Environmental West Virginia Mine Drainage.

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Presentation transcript:

Sustained Treatment of AMD Containing Al and Fe 3+ with Limestone Aggregate Neil Wolfe and Robert Hedin Hedin Environmental West Virginia Mine Drainage Task Force Meeting March 2011

Limestone Advantages Limited solubility –cannot over-treat –Can install years of treatment capacity Can store on site in open piles without loss Not hazardous Less than 20% the cost of lime and caustic alternatives

Limestone Disadvantage When exposed to acidic water containing Al and Fe 3+, solids quickly form Solids foul limestone aggregate, greatly decreasing its effectiveness

Project Goals Understand why the effectiveness of limestone treatment is reduced by Al and Fe solids. Develop a treatment approach that can overcome these limitations and provide sustainable treatment of low pH AMD with limestone aggregate

pH 2.9 Acidity, 290 mg/L Al, 29 mg/L Fe, 8 mg/L Mn, 15 mg/L Two parallel 27 m 3 roll off containers filled with ~30 tons limestone Construction of Experimental Flush Units Agri Drain SDS “Small” limestone East Box West Box

Experimental Measure performance of limestone units –Influent and effluent samples pH, alkalinity, acidity, sulfate Total and dissolved Al, Fe, and Mn Vary operational parameters –Flow rate –Water level in limestone bed –Drainage trigger (time, water level, chemistry)

Solids Solids form when alkaline conditions arising from calcite dissolution cause: Al 3+  Al(OH) 3 Fe 3+  Fe(OH) 3 Solids accumulate in the aggregate in two manners

Solids accumulate in pores

Solids form scale on limestone

Scale flakes off revealing clean LS surface

What happens when a limestone bed is drained empty? Solids in aggregate pores are flushed away –porosity is restored Some scales are dislodged, exposing clean limestone surface –Alkalinity generation is restored

Treatment Goal Identify the retention time necessary to achieve treatment goals Identify the bed drainage schedule that maintains treatment effectiveness

Long-term alkalinity generation

LocationpHAcidFeAlMn Influent Effluent *2.9*3.0** Metals are mg/L and acidity is mg/L CaCO 3 *Suspended solid; **dissolved Average chemistry since change to 1 gpm and 1/wk drainage (28 months)

Mn removal, flow 1 gpm, drain 1/wk

Solids accounting for the West Box

Solids accumulation will eventually affect calcite dissolution and bed performance: Limestone must be either replaced or cleaned

Cleaning limestone bed with an excavator and AMD flow

Cleaned limestone aggregate Cleaning cost: $5/ton New limestone costs $22/ton

West box performance as of March ton CaCO 3 net alkalinity generation 10% of installed limestone has dissolved

West box performance as of March 2011 At $40/ton LS installed (with settling pond) –$408/ton CaCO 3 net alkalinity Comparative costs –Anna S VFP system, $ /ton CaCO 3 –NaOH system, $1,500 – 2,500/ton CaCO 3 –lime plant, $ /ton CaCO 3 –Stream dosing (lime), $ /ton CaCO 3

Summary 1.Effective treatment of acidic Al and Fe 3+ contaminated mine water can be achieved with limestone aggregate as long as the bed is regularly drained empty. 2.Fouled limestone aggregate can be cleaned and its alkalinity generation restored. 3.Sustainable Mn removal can be achieved at pH levels between 6.5 and 7.0.

Scootac system (2010) Renovation of existing VFP –735 tons LS aggregate and 223 CY organic substrate Installation of parallel DLB –1,000 tons LS aggregate –AgriDrain SDS Polishing pond Flow distribution

Scootac system, Nov 2010 – Mar 2011 FlowpHAcidAlkAlMnFeSO 4 gpmmg/L CaCO 3 mg/L Raw Drainable LS Bed < Vertical Flow Pond < Polishing Pondna

Scootac system (on line Nov 2010)

Questions? Insert good photo or figure