TRT Leak Repair Anatoli Romaniouk, 22.05.2013 1. EC leak tests Side C Side A 2.

Slides:



Advertisements
Similar presentations
FDR 10/01 Jason Tarrant CLRC1 SCT EC Thermal Enclosure (TE) l Thermal Enclosure Function: »Make End-cap thermally neutral »Condensation free exterior »Containment.
Advertisements

BumperBot uses two contact switches to go through a labyrinth. Bumper.
Installation. Indoor Unit Installation Typical Installation.
Engineering Division 1 HFT Middle Support Cylinder Eric Anderssen, LBNL.
Summery of Cooling System Teflon Leaks* *This is independent of the internal problems Rob Pisani.
PEUGEOT 206 INSTALLATION 99’— 05’ TU5JP4
A.Nichols CLRC1 SCT HEX PRR ( ) Layout & Installation of Barrel off-detector HEX circuits From barrel cooling loop to PPB1 l Barrel Hex is a plain.
IR2 and IR4 Summary PEP-II meeting Jan. 23, 2006 M. Sullivan.
Installation. Indoor Unit Installation Typical Installation.
TP4-ENERSOL-TD/PV double function
SPACE FRAME Interface between the LGT and the IST 21/06/2011 Marco Ciapetti.
Caterpillar CaterpillarBot is a robot that can pass the bumpy road by using caterpillar.
Comparison of cooling services at barrel end Description SCT Barrel Upgrade ID barrel one end one end Total number of staves/rows 176 Staves/rows serviced.
Installation. Indoor Unit Installation Typical Installation.
Chiho Wang ATLAS TRT Duke University CERN, Feb TRT Barrel assembly status & schedule Feb. 9, 2005.
Ciemat Mechanical Structure Proposal for a DHCAL m 3 Prototype. Enrique Calvo Alamillo Paris
Ron Madaras, LBL U.S. Pixel Meeting, SCIPP, July 9-10, 2003 Patch Panel 1 (PP1) Brief Review Cost and Effort Estimate.
TRT Leak Repair Anatoli Romaniouk, EC leak tests Side C Side A 2.
Installation and Commissioning Planning Leslie Camilleri Calorimeter Commissioning Meeting 5 th September 2006.
M. Gilchriese - November 12, 1998 Status Report on Outer Support Frame W. Miller Hytec, Inc E. Anderssen, D. Bintinger, M. Gilchriese LBNL.
CEDAR Opening 26/03/2012-FH1. Cedar Overview 26/03/2012-FH2.
IPN Lyon ILD Mechanical structure April 2012 DHCAL Assembly, Tooling, Cooling J.C Ianigro - IPN Lyon -
18 July 2006A.Ciocio -SCTSG1 SCT Services Installation ID week full report (July 4) SCT Cables Web page
ATLAS TRT CO 2 cooling system project status Beaufort 12: “Hurricane” (>119 km/h) Saffir-Simpson 5: “catastrophic damage” (>250 km/h) (CO 2 distribution.
JCOV 24 NOVEMBER 2005 J.Godlewski EP-ATI 1 JCOV NOVEMBER 2005 ATLAS cooling systems installation plans Jan Godlewski CERN EP-ATI The H.Niewodniczanski.
CONSTRUCTION Andrea d'AURIA PH / DT-DI / GAS.
Straw Working Group Status assembly at CERN Plans 10/2/14Straw WG.
Test beam setup: status report 31/03/2009 M. Alfonsi (CERN)
TRT active gas leak repairing F. Perez, C. Degeorge, S. Katunin, I. Zhukov, V. Myalkovskiy, S. Konovalov, A. Romaniouk, H. Danielsson, A. Catinaccio, K.
Anatoli Romaniouk TRT Introduction TRT in ATLAS p. 2-4TRT in ATLAS p. 2-4 TRT design p. 5-7TRT design p. 5-7 TRT operation principles p. 8-9TRT operation.
Argontube Detector design Laffranchi Marco, Meregaglia Anselmo, Messina Marcello, Rubbia Andre’ Bern,
Test Tube Activities at Ohio State (8/5/03) Two (very useful) sub-group meetings after last weekly meeting –Mechanics (Bill, Lu, Mark, Jim, Charlie, Klaus)
Chiho Wang Duke University 1 TRT Barrel integration Status / Schedule Chiho Wang.
LHCb Experimental Area Meeting V. Bobillier1 Earth network in UX85 experimental cavern.
Compressor Replacement – ODU
1/5 ECAL/HCAL Front-end status Calorimeter Meeting Frédéric Machefert Wednesday February 9 th, 2011.
M. Gilchriese Pixel Update October 3, M. Gilchriese 2 Outline Barrel status and repair strategy Revised ATLAS installation schedule Finishing pixel.
Alpine pixel layout Integration progress Teddy Todorov For the ATLAS-LAPP group AUW Integration meeting 20/11/2012.
SLHC Engineering Upgrade FCAL Remove-Install step by step procedure. Mircea Cadabeschi-University of Toronto March 01,
IBL Mock up Mounting procedure V.2 François-Xavier Nuiry Simon Feigl
IPN Lyon ILD integration April 2015 Jean-Christophe Ianigro & Imad Laktineh - IPN Lyon -
V. Bobillier1 Cable installation status.
Special interventions Status of production and QC Nicolas Bourcey TE-MSC-MDT Fourth LHC Splice Review November 2013.
Chiho Wang ATLAS TRT Duke University CERN, Sep Barrel integration status.
Beampipe Installation Status Ray Veness For the Beampipe team in AT/VAC and TS-MME.
T2 Status Report IP5 Installation Future plans. IP5 installation The mechanical structure has shown problems on installation and should be changed slightly.
February 26 th 2013Muon LS1 operation meeting1 Muon LS1 Status Outline Recap of last week P1 weekly schedule Muon related activities Open issues and discussions.
IPN Lyon ILD Mechanical structure February 2015 Design, Integration & Services J.C Ianigro - IPN Lyon -
Atlas status report. LHC Cooldown Status LHC is proceeding with the cooldown and the hardware commissioning L.Evans is asking the experiments to close.
TRT (and a bit beyond) – Overview 1. TRT Desynchronization – [206248: 1 -> : 533), elogelog – ROD firmware issue Reverted to the before-the-TS settings.
- PROPOSAL FOR A SOLUTION OF A “STRAW MODULE” INTEGRATION - INFN-LNF - SPAS -STRAW MODULES INTEGRATION- INFN-LNF-SPAS- December D. Orecchini – P.
USCMS Pixel PMG, Nov 29, Mechanics Status Disks, ½ Service Cylinders Installation USCMS FPIX FNAL PMG Joe Howell Bruno Gobbi Nov. 29, 2006.
1 04 April 2007 L. Roy Detector Safety System for infrastructure - General fire detection (barracks, cavern) - Sniffer system (smoke detection above the.
BGV 23-feb-2016CERNMassimiliano Ferro-Luzzi 1 BGV cooling : status and plans reporting on behalf of EN-CV (Sylvain Nichilo & Olivier Crespo-Lopez)
Removing the VTPC from the VERTEX magnets
- STT LAYOUT - SECTOR F SECTOR A SECTOR B SECTOR E SECTOR D SECTOR C
Very preliminary draft
Services – First Considerations Sigi Wenig / Nicolas Massol ATLAS Tracker Upgrade Workshop Valencia December 2007 Existing services (in cryostat.
Preliminary Y-chamber specifications – First draft
Easycliner (Motorized Version) Assembly Instruction
Integration issues at IHEP
Hall A Target Status 9/27/16 Dave Meekins.
Flexible lines assembly
First of all we will remind some numbers:
ATL-IC-ES new version available - approval starts
Final Design CGEM Workshop HIEP, 14/03/2017 M. Melchiorri - INFN FE.
Reader Swap out Guide.
Pipe fitting Threads on pipe fittings are tapered and rely on the stress generated by forcing the tapered threads of the male half of the fitting.
IR Beam Transport Status
Presentation transcript:

TRT Leak Repair Anatoli Romaniouk,

EC leak tests Side C Side A 2

Location of the pipes with leaks А6 PPF1 connector А4 Bracket А2 Detector side А1 PPF1 connector B3 Bracket EC Side C 3 B5 Bracket А3 Bracket A2 OUT F mm Ch. 2 Leak 0.3 l/h A3 OUT F mm Ch. 3 Leak 0.3 l/h A4 OUT F mm Ch. 4 Leak huge A6 OUT F mm Ch. 6 Leak huge A1 OUT F mm Ch. 1 Leak 17l/h B5 OUT F mm Ch. 11 Leak 0.3l/h B3 OUT F mm Ch. 9 Leak 2 l/h

EC Side C: Endoscope study Pipes were cut and were studied with endoscope from inside 4

A1 crack along the pipe (PPF1 connector) 5

A4 PPF1 bracket.

Detector connector 7

This pipe should be repaired To go inside we need to open some accesses Repair should be done also here (PPF1 area) 8

9 Example how pipes installed on the calorimeter flange

10 EC wheel type A connectivity Electronics Gas manifold Gas Straws/radiator Electronics Gas manifold Gas Straws/radiator Gas IN Gas OUTPEEK pipes shown in pink Places of stress

EC: on detector connection

12 PEEK pipe termination Most probable location of leaks

Repair at the detector level Nut PEEK pipe Most probable places of leaks Insert Steel pipe Polyurethane joint Connector Removable steel road

14 Example how pipes installed on the calorimeter flange

15 Repair status TRT WheelRepair and testsComments A1 A2Done, OKLeak fixed A3Done, OKLeak fixed A4Done, failedLarge, Repair is OK but leak in the other place A5Done, OKNo leak before A6Done, partially failedLeak reduced but still large. Repair is OK but there is still leak in the other place B1Done, OKNo leak before B2Done OKNo leak before B3Done, failedLeak still at the level of 2.5 l/h (can be controlled) B4Done OKLeak was small, now no remarkable leak B5Done, failedLeak still at the level of 0.25 l/h (can be controlled) B6 B7 B8

16 Next steps: Today - try to go outside of the tube ( A4 and A6) and see what can be done at the place of connection. End of the week - Close C side (if no additional repair can be made) and start working with side A. When side A will be available to start preparatory work?