Radiation Safety Management KHNP Lee Eung-Il HANUL Unit4 Steam Generator Replacement.

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Radiation Safety Management KHNP Lee Eung-Il HANUL Unit4 Steam Generator Replacement

1 Hanul (#1,2,3,4,5,6)) Shin-hanul (#1,2) Shin-hanul (#3,4) Kori (#1,2,3,4) Shin-Kori (#1,2) Shin-Kori (#3,4) Shin-Kori (#5,6) Yonggwang (#1,2,3,4,5,6) Wolsong (#1,2,3,4) Shin-Wolsong (#1) Shin-Wolsong (#2) Seoul Hanbit(#1,2,3,4,5,6) In operation under construction planning 23 units (20,716 MW) 5 units (6,600MW) 4 units (5,600 MW)

CONTENTS Main process 2 2 Summary Radiation safety management Radioactive waste management

3 1. SUMMARY HANUL Unit 4  business operated day : 31, December, 1999  type : PWR(pressurized-water reactor)  reactor shutdown day : 9th, September, 2011 Replacement Subject : two steam generators  reason : excess of acceptance rate of steam generator tube plugging  period of replacement : ~ 8.14(97D) Condition

4 2. MAIN PROCESS MAY

5 Installation of the temporary power supply cable 1 1 Installation of shielding Installation of shielding materials & fixing device materials & fixing device 5 5 Installation of the scaffold & removal of insulation 4 4 cutting the main cutting the main steam pipes 6 6 Installation of the Installation of the refueling pool cover refueling pool cover 2 2 Installation of the Installation of the temporary auxiliary crane MAIN PROCESS

6 Installation of the rail Installation of the rail 10 Installation of the lifting equipment(HLU/TLD) 11 disconnecting of SG lower fixture 12 marking the cutting marking the cutting part of RCS pipes part of RCS pipes 9 9 disconnecting of disconnecting of SG upper fixture SG upper fixture 8 8 disassembling of the PWR MAIN PROCESS

7 cutting the RCS pipes 13 coating the SG surface coating the SG surface 14 preparation of preparation of taking out SG 15 Taking out the SG 16 preservation of the SG into OSGSF 17 decontamination of the decontamination of the inside RCS end pipes MAIN PROCESS

8 RCS pipes processing RCS pipes processing the cutting plane 19 bringing of the new SG into RCB 21 RCS pipes inside welding 24 fitting up of the new SG on the RCS pipes 22 new SG and RCS pipes outside welding new SG and RCS pipes outside welding 23 new SG transportation new SG transportation MAIN PROCESS

9 Inspection & removal of foreign materials 25 welding of welding of the MS/FW pipes 26 Installation of the Installation of the insulation materials insulation materials 27 loading the nuclear loading the nuclearfuel 28 reactor start-up reactor start-up 29 synchronization & connection synchronization & connection MAIN PROCESS

10 3. RADIATION SAFTY MANAGEMENT collective dose  goal : 210 man-mSv, result : 177 man-mSv individual dose : 16 mSv/yr  unavoidable case of excess exposure: 20 mSv/yr  legal requirement : 50 mSv/yr, 100 mSv/5year management goal 1) Woker exposure dose management

11 3. RADIATION SAFTY MANAGEMENT ○ Exposure dose of the major work NOMajor workgoalresult 1RCS pipes cutting, grinding, welding RCS pipes clamping, supporting1514 3RCS pipes inside decontaminating SG support fixture, platform removal and installation Shielding materials installation and removal Heat insulation materials of SG, RCS pipes removal and installation others total

12 2) Method of reducing exposure radiation dose for worker delay the draining of SG primary and secondary coolant conducting pre-mock up training for major radiation work radiation shielding : installation of temporary lead shielding materials for RCS pipes and lead shielding structure for OSG installation of the movable air cleaning unit monitoring continually the air contamination level(movable continuous air contamination monitor) decontamination of the inside of RCS end pipes measurement of radiation and radioactivity for a day, of work 3. RADIATION SAFTY MANAGEMENT

13 RCS and MS/MW pipes cutting machine RCS pipes welding cutting welding 3. RADIATION SAFTY MANAGEMENT ○ Conducting pre-mock up training for major radiation tasks

14 shielding plug pipe end decontamination(PED) shielding decontamination 3. RADIATION SAFTY MANAGEMENT ○ Conducting pre-mock up training for major radiation tasks

15 transportation 3. RADIATION SAFTY MANAGEMENT SG weight : 546 ton, total weight : 637 ton(included saddle, lashing) Mock up weight : 730 ton ○ Conducting pre-mock up training for major radiation tasks

16 ○ Radiation shielding(pipes and object) 3. RADIATION SAFTY MANAGEMENT

17 ○ Radiation dose rate after shielding (mSv/h) ※ total quantity needed of lead material : 1,150 sheets locationInstallation place mSv/h beforeafter RCB 86’ Reactor drain pipe Refueling Pool drain pipe RCB 100’ SG hot leg pipe SG cold leg pipe RTD pipe RCB 116’SG H/L→PZR Surge Line RADIATION SAFTY MANAGEMENT

18 ○ Radiation shielding(SG lead shielding structure) 3. RADIATION SAFTY MANAGEMENT

19 outside surface of transporting object : 2 mSv/h outside surface of transporting vehicle from 2m : 0.1 mSv/h surface contamination : below surface contamination control limits  surface contamination control limits : 4 Bq/cm 2 SG transportation terms outside surface of transport object : 3.1 uSv/h outside surface of transport vehicle from 2m : 2.84 uSv/h(→0.44 uSv/h) surface contamination : natural background radiation level Measured value 3. RADIATION SAFTY MANAGEMENT

20 ○ Installation of the movable air cleaning unit 3. RADIATION SAFTY MANAGEMENT capacity : 2,000cfm, 750cfm, 560cfm

21 ○ Monitoring continually air contamination Continual air monitor Grab sampler 3. RADIATION SAFTY MANAGEMENT

22 ○ Pipe end decontamination(PED) of RCS 3. RADIATION SAFTY MANAGEMENT

23 4. RADIOACTIVE WASTE MANAGEMENT typeironcottonpapervinylplasticrubberinsulation amount9,4161, , ,0732,100 unit : kg ○ Generated amount of radioactive waste ○ Method of reducing radioactive waste iron  high level contamination : storage of 200 ℓ drum  low level contamination : disposal after long term storage rest of radioactive waste : storage of 200 ℓ drum