3/19/09
Animal Motor Works (AMW) K475WW High Power Rocket Motor. 54 mm casing, 40.3 cm long, 2.9 seconds burn time, 1394 N-sec total impulse, and Newtons average thrust.
Rocket flight stability in Rocksim static margin diagram The stability margin is 3.45
Thrust to weight motor selection in flight simulation 474 N average thrust 221 oz
Rail exit velocity Launch guide length: In. Velocity at launch guide departure: 60.3 ft/s
Parachute sizes and descent rates The drogue parachute parachute was built by Ernie Puckett and descent rate is 88 ft/s. The hemispherical main parachute was donated by Edward Warinski of Alpha Hybrids. Velocity at landing: Vertical: 17 ft/s. 54inches in diameter with 8 inch spill hole.
Test plans and procedures The first flight of our scale model occurred January 17, The full scale rocket was flown on March 14, 2009 Video footage from March 28:
Full-sized final rocket flight test
Dual deployment avionics test We successfully tested the avionics in both rockets and we are using the same equipment in the full sized rocket with an added G-Wiz flight computer back up system.
Ejection charge amount test We used.75 grams of black powder in the scaled down rocket. We calculated this using the uroc.org black powder calculation website: =628 =628 We used 1.4 grams of black powder for the drogue parachute and 1.7 grams of black powder for the main parachute. We used the black powder calculator on:
Payload integration feasibility Camera bay hatch. "Record" access hole added to hood. Transmitting GPS donated as a loaner. Small logging GPS and a sonic locator optional.