Atsuto Suzuki (KEK). 1.Energy Management at KEK 2.Improve Efficiency of Power Consumption in Accelerator Operation 2.1 How to Improve RF Efficiency 2.2.

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Presentation transcript:

Atsuto Suzuki (KEK)

1.Energy Management at KEK 2.Improve Efficiency of Power Consumption in Accelerator Operation 2.1 How to Improve RF Efficiency 2.2 How to Save Power in Cryogenics 2.3 How to Recover Beam Dump Energy 3.Improve Power Storage to Reuse 4.Summary

J-PARC Energy Storage for Power Fluctuation Compensation at J-PARC MR MR Power Amplitude of J-PARC-MR Operation Cycle J-PARC MR Reputation (sec.)3.64 Power (MW)105 Line Voltage (kV)66/22/6.6 Compensation TypeFly Wheel : 51 MVA SMES : 90 MVA A MW (1 – 4 sec. cycle) Developing new MGs with large capacitor energy storage: F. Kurimoto’s talk

20 MJ Advanced Large Liquid Crystal plant in Kameyama since MJ Kinetic Energy Storage (Fly Wheel) in Okinawa Fly -Wheel and SMES Status in Japan

serious issue for ILC

Improve efficiency Increase recovery Infrastructure : 50 MW RF System : 70 MW Cryogenics : 70 MW Beam Dump : 10 MW 200 MW loss rate 50 % : 25 MW 50 % : 25 MW 50 % : 35 MW 50 % : 35 MW 90 % : 60 MW 90 % : 60 MW 100 % : 10 MW ~ 130 MW ~ 130 MW Power Balance of Consumption and Loss in ILC Obligation to Us

2.1 How to Improve RF Efficiency R&D of CPD (Collector Potential Depression) Klystron CPD is an energy-saving scheme that recovers the kinetic energy of the spent electrons after generating rf power. Conventional collector Schematic diagram of CPD collector

Simplified Schematic Concept Potential denotes the electron potential energy, eV. For simplicity, input and intermediate cavities are omitted here and the anode potential is set to zero. Potential & Electron Energy Cathode Anode Output cavity Collector RF Potential in the KlystronElectron Energy With CPD E0E0 EcEc CPD gap UkUk UcUc E1E1 Potential & Electron Energy Cathode Anode Output cavity Collector RF Potential in the Klystron Electron Energy Without CPD E0E0 UkUk UcUc EcEc E1E1 Efficiency of RF Conversion (40-50) % Heat Loss Beam Deceleration Energy Recovery/Reuse

(I) Energy spread The spent electron beam has large energy spread through electromagnetic interaction in the cavities. Therefore, the collector potential cannot be increased beyond the lower limit of energy distribution of the spent electron beam, otherwise backward electrons hit the cavities or the gun, and then deteriorate the klystron performance. Issues must be addressed for CPD Klystron Saturated: 1 MW out Unsaturated: 200 kW out E 0 = 90keV (II) Pulse-to-DC conversion The spent electron beam is longitudinally bunched, so that pulsed voltage is induced on the collector. An adequate pulse-to-DC converter has to be implemented. (III) RF Leakage CPD klystron has to be equipped with an insulator between the collector and the body column in order to apply CPD voltage to the collector. Thus, it would be possible for the CPD klystron to leak rf power out more or less from the insulator. Ceramic Insulator Output Coupler Collector

Present Status of R&D R&D Schedule : Modification of an existing klystron to CPD klystron (already done) : until then, preparation and commissioning of the test station ~2014: Verification of klystron operation without CPD ~2015: Measurement of rf leakage from the gap between the body column and the collector (with no CPD voltage applied) Measurement of induced pulse voltage on the collector with CPD ~2017: Test of rectification by Marx circuit Integration test of the proof-of-principle of CPD operation R&D Schedule : Modification of an existing klystron to CPD klystron (already done) : until then, preparation and commissioning of the test station ~2014: Verification of klystron operation without CPD ~2015: Measurement of rf leakage from the gap between the body column and the collector (with no CPD voltage applied) Measurement of induced pulse voltage on the collector with CPD ~2017: Test of rectification by Marx circuit Integration test of the proof-of-principle of CPD operation Recycled components electron gun input cavity intemediate cavities Newly fabricated components collector ceramic insulator output cavity output coupler Target proof-of-principle of CPD in the unsaturated region (a maximum rf power of 500 kW) using a KEKB 1.2MW-klystron Target proof-of-principle of CPD in the unsaturated region (a maximum rf power of 500 kW) using a KEKB 1.2MW-klystron 80 % efficiency

Multi(6) – Beam Klystron (MBK) for 26 Cavities for ILC Frequency1.3 GHz Peak power10 MW Pulse width1.6 ms Rep. rate5 Hz Average power78 kW Efficiency65 % Gain47dB BW (- 1dB)3 MHz Voltage120 kV Current140 A Lifetime40,000 h  The design goal is to achieve 10 MW peak power with 65 % efficiency at 1.5 ms pulse length at 10 Hz repetition rates.  MBK has 6 low-perveance beams operated at low voltage of 115 kV for 10 MW to enable a higher efficiency than a single-beam klystron.

Completely Old/New Idea for Klystron Synchrotron Radiation Electron Tube RF output Cathode Synchrotron radiation from small bend Bunched Electron Beam 1.3GHz Electron Gun Klystron – > 90% efficiency (small transient time factor by short bunch) – Stabled by space charge limit operation – Drivn from low charge low energy 1.3GHz electron beam (1/10 klystron ?) – Very low cost and long lifetime – Low cost beam line – No switch, only HV & capacitor Advantages

2.2 How to Save Power in Cryogenics Cryogenics/Stirling Cryocooler High temperature operation – Klystron collector – RF Dummy load

Multiple Stirling Cooling System 2 Stage-Stiling Cryocooler 1 st stage 2 nd stage thermal link compressor cold head

2.3 How to Recover Beam Dump Energy ( ~ 10 MW)  Recover Beam Energy  Reduce Radio-Activation

Noble Gas Dump  About 1km of a noble gas (Ar looks the most promising) enclosed in a water cooled iron jacket (transport the heat).  This gas dump design may ease some issues such as radiolysis and tritium production.  Issue : particle beam heating of the gas and ionization effects. Water Dump Water Vortex Dump (25 m long x 15 m height for 1 TeV) SLAC Dump for 800 kW  Issue : shock wave management  Issue : management of tritium gas and tritiated water in vapor form

 The deceleration distance in the underdense plasma is 3 orders of magnitude smaller than the stopping in condensed matter.  The muon fluence is highly peaked in the forward direction. Plasma Deceleration Dumping 10 cm for 100 GeV Use Collective Fields of Plasmas for Deceleration

here & ILC  T ≈ 50  m,  L ≈ 3  T ≈ 150  m Collective Stopping Power for ILC (electron bunch)  L = 10 m for Li gas Next Trials  Experiment of Proof-of-Principle  Deposit mechanism of Wake-Field energy

Store the surplus electric energy as thermal energy Storage of Electric Energy as Heat in Iron Electric Energy 100 MW x 1 0 hours E = 100 M J / sec x 3600 sec / hr x 10 hr = 3600 GJ 10 m 3 x 10 3 m 3 ~ 1.7 GJ x ~ 5100 GJ m Heat Capacity Iron vs. Water Heat Capacity of Iron Heat Capacity of Water Storage of Thermal Energy

how to keep iron heat ILC Tunnel Blast Furnace Fire Brick

ILC Improve Efficiency Recover Energy Reuse Energy Reuse Energy Stand Alone Energy System

 The muon fluence is highly peaked in the forward direction. Beam dump  Injection Fixed Field Alternating Gradient Accelerator FFAG Ring RF Extraction Extraction  Usage No Extraction  Decay 