NuMI Target Hall Performance/Plans Jim Hylen DOE Tevatron Operations Review March 27, 2007.

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Presentation transcript:

NuMI Target Hall Performance/Plans Jim Hylen DOE Tevatron Operations Review March 27, 2007

2007 DOE Tevatron Operations Review – Jim Hylen 2 Outline  Overview of target hall and target/horn experience  Summary of problems causing 1 day or more downtime, and corrective actions underway  (back-up slides describing individual problems)  Spares status  Plans for target with evolving beam conditions

2007 DOE Tevatron Operations Review – Jim Hylen 3 How NuMI beam is produced Design for 0.4 MW proton beam

2007 DOE Tevatron Operations Review – Jim Hylen 4 Target for Low Energy Neutrino Spectrum Graphite Fin Core 6.4 mm wide Water cooling tube Backing target out of horn produces neutrinos at higher energies Fits within the horn.

2007 DOE Tevatron Operations Review – Jim Hylen 5 Experience with the NuMI Target Max. Proton/spill Max. Beam Power Integrated Protons on Target Target Design specification 40e12 p.p.p.400 kW370 e18 p.o.t. lifetime 1 st target Before leak 25e12 p.p.p. 11e12 day before leak 69 kW 0.7 e18 p.o.t. 1 st target After leak 30e12 p.p.p.270 kW 158 e18 p.o.t. 2nd target40e12 p.p.p.320 kW 105 e18 p.o.t. 1 st Target took beam for over a year, 820 MWhr integrated beam power. Two problems: water leak soon after turn-on; back-pressure with Helium to keep water out target motion drive shaft froze up after year of operation – stuck in H.E. focus 2 nd Target is running (no leak)

2007 DOE Tevatron Operations Review – Jim Hylen 6 Magnetic Horns  focused by toroidal field between conductors  3 Tesla peak field  200 kA peak current  To be focused,   must penetrate inner conductor  Low mass (2 mm thick nickel-coated aluminum)  Parabolic shape produces “Lens” field (Pt kick  Radius)  Water spray cooling on inner and outer conductors  Inner conductor dominated by joule heating  Outer conductor dominated by beam heating  3 m long focusing region  Achieved ~ 0.1 mm radial tolerance after weld Outer Conductor Inner Conductor Stripline Drain Insulating Ring Water Spray Nozzle   

2007 DOE Tevatron Operations Review – Jim Hylen 7 Horn Inner conductors Parabolic inner conductors: 3 Tesla max. magnetic field 3 m active length each horn Inner conductors welded together at FNAL by lead engineer Kris Anderson

2007 DOE Tevatron Operations Review – Jim Hylen 8 NuMI Horns Experience Horns in target hall June st run with beam Jan Accumulated: 15 Million pulses 1,350 MWhr integrated beam power Still running with first set of horns

2007 DOE Tevatron Operations Review – Jim Hylen 9 Target Hall during construction 1/2 of the 8000 tons of shielding is installed

2007 DOE Tevatron Operations Review – Jim Hylen 10 Work cell Target module in beam-line 1st target being removed Work cell Target module in beam-line 1st target being removed

2007 DOE Tevatron Operations Review – Jim Hylen 11 NuMI work cell for radio-activated components Shown during test-assembly above ground Lead-glass windows (not shown) Remote controlled door Remotely installable top shielding

2007 DOE Tevatron Operations Review – Jim Hylen 12 All NuMI target hall beam components and innermost shield layers are installed /removed remotely with crane and cameras Crane includes remote hook rotation. Steel shielding block being moved.

2007 DOE Tevatron Operations Review – Jim Hylen 13 Big Picture of Maintenance  NuMI target hall is a difficult system  High radiation forces remote handling repairs take a long time  Target hall is nasty environment E.g. humidity has PH of 2.6, very corrosive Limited list of materials are rad-hard enough  Interventions are time-consuming Access to components requires 1 shift just to put electronics back on target hall crane Must un-stack, then re-seal shielding each access Components are an order of magnitude larger than Pbar’s Achieving high up-time requires design of robust components  Biggest current concern:  Producing an adequate supply of spare horns Usually replacement takes less time than repair

2007 DOE Tevatron Operations Review – Jim Hylen 14 NuMI Performance – POT/week Horn 2 ground fault Tritium Mitigation Accelerator Shut Down Horn 1 cooling spray clog Horn 1 water line repair and target replacement Beam-line magnet replacement Target pile chiller replacement Accelerator down

2007 DOE Tevatron Operations Review – Jim Hylen 15 Up (513) and down (83) days 5/1/05 – 3/22/07 86% / 74% efficiency excluding / including sched. shutdown DaysDescription (**non-recurring)Long term corrective action 513Up for beam 95Accelerator scheduled down 25Horn cooling spray clog **Check valves, filters on skids 14Horn water line repairEliminate braze on spares 14Target motion frozenGraphalloy bushing on spare 10Horn ground faultPin feet, float modules 8Tritium mitigation **Condensate sys./dehumidifiers 6Replace NuMI beam-line magnet 4Replace accelerator magnet 2Replace pile chiller compressorNew hot spare chiller unit

2007 DOE Tevatron Operations Review – Jim Hylen 16 Other long term actions  Corrosion protection  Improve dehumidification of target pile Planned installation summer 2007  Selection of materials E.g. stainless sheathing instead of nickel coating of shielding on remote electrical clamp for spares  Accelerate production of spares  Batch process horns Doing several at once is much more efficient  Engineer hired specifically for spare horn welding  Tech. assigned specifically to track parts

2007 DOE Tevatron Operations Review – Jim Hylen 17 Horn spray flowmeter with beads Horn nozzle for inner conductor is eliptical ~40 mils short direction (48 total) outer conductor nozzles round, 25 mils diameter (19 total) plus two side-spray nozzles June 30, 2006, resin beads from deionization bottle clogged the water spray lines on Horn 1 New, uncontaminated beads Beads are ~ 20 mils diameter

2007 DOE Tevatron Operations Review – Jim Hylen 18 The gravity un-assisted check valve When water skid was turned off for maintenance, beads floated backwards through improperly mounted check valve

2007 DOE Tevatron Operations Review – Jim Hylen 19 Cleaning Out Resin Beads Fan push, water-in-barrel filter, vacuum suck

2007 DOE Tevatron Operations Review – Jim Hylen 20 Have brazed ceramic electrical insulators on horn water lines They are strain-relieved with invar+ceramic clam-shells On horn 1, developed a 7gal/day water leak on line to spray header On horn 2, leak on suction line drew air in, reducing amount of water ejector pump could remove from horn collection tank Both ceramic sections were successfully replaced Speculate braze corrodes… planning to switch from brazed to a shrink-fit ceramic/steel connection for spare horns Two horn water system leaks: Horn 2 in February 2006, Horn 1 in August 2006

2007 DOE Tevatron Operations Review – Jim Hylen r/hr ( 0.75 Sv/hr) on contact 35 r/hr ( 0.35 Sv/hr) at 1 foot Repair people got weekly dose limit in a few seconds High dose rates made Horn 1 ceramic replacement challenging

2007 DOE Tevatron Operations Review – Jim Hylen 22 Built an extension of the work-cell with window for work Shielding for Horn 1 ceramic repair job ( Horn is in work-cell, behind the door )

2007 DOE Tevatron Operations Review – Jim Hylen 23 Mock-up and practice for repair Plan, time, and practice, practice, practice repair Needed to undo two Swagelok fittings, remove old section, insert new section, and tighten two fittings. Time est: 2 min. of actual work in slot Dose for this “2 min.” job was 371 mr, (3.7 mSv) divided over ~10 people. The rest of job is in much lower radiation field, but dose can be non-negligible due to time involved.

2007 DOE Tevatron Operations Review – Jim Hylen 24 Frozen drive shaft on target motion system On 2 nd carrier - Light lube of nuclear grade anti-seize compound Old jammed pillow-block After month-long test in High Energy position drive shaft will not rotate to move target into Low Energy position On target carrier #3, change to Graphalloy bushing

2007 DOE Tevatron Operations Review – Jim Hylen 25 Horn 2 ground fault -- loose foot on horn Owl shift Thurs. Sept. 29, 2005 intermittent horn trips. Owl shift Sat. Oct. 1, hard ground fault of 1 ohm. -removing stripline fingers Horn 2 + stripline block -when Horn 2 moved to work cell ground fault cleared -foot left behind in chase, nut had vibrated off -scorch marks seen under foot Moved old foot, installed new foot Horn 2 before beam 1.5 inch clearance foot to floor

2007 DOE Tevatron Operations Review – Jim Hylen 26 Horn 1, after a year of beam Horn is corroding – eventually will have to replace it

2007 DOE Tevatron Operations Review – Jim Hylen 27 Spares Status – Horns and target

2007 DOE Tevatron Operations Review – Jim Hylen 28 Plan for target for evolving beam condition Existing target was designed for 4.0e13 p/pulse, 400kW  After summer shutdown, slip-stacking may provide up to 4.5e e13 p/pulse, 400 kW (when pbar source not running)  By increasing beam spot size to 1.2 mm RMS for 4.5e13, will have same stress as current 1.0 mm RMS for 4.0e13 on target  Have tested larger spot size, baffle scraping by beam still fine  Preliminary Monte Carlo indicates negligible impact on neutrino spectrum

2007 DOE Tevatron Operations Review – Jim Hylen 29 Plan for target for evolving beam condition For NOVA experiment (2011), target no longer needs to fit in horn  M.E. target design  With ANU sub-project, beam specification is 4.9e13 p/pulse, 700 kW  By increasing beam spot size to 1.3 mm RMS, will have same stress as current 1.0 mm RMS for 4.0e13 on target  Moving water cooling further from beam-spot reduces water-hammer  Still work to do on window and outer casing cooling, but does not appear to be any show-stoppers

2007 DOE Tevatron Operations Review – Jim Hylen 30 Medium Energy Target for NOVA running IHEP Design 120 cm

2007 DOE Tevatron Operations Review – Jim Hylen 31 Plan for target for evolving beam condition A possible next stage for beam after ANU is to re-use Accumulator Ring Plan to use essentially same NOVA M.E. target design  With Accumulator, beam specification could be 8.3e13 p/pulse, 1200 kW  By increasing beam spot size to 1.5 mm RMS, would have calculated stress safety factor of x1.4 on graphite  Still work to do on window and outer casing cooling, but appears doable