Coupler Multipactor Studies F. Wang, B. Rusnak, C. Adolphsen, C. Nantista, G. Bowden, Lixin Ge.

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Presentation transcript:

Coupler Multipactor Studies F. Wang, B. Rusnak, C. Adolphsen, C. Nantista, G. Bowden, Lixin Ge

SLAC Coupler Test Stand - Evaluate Parts Individually An SRF coupler is a complex integration of many components When a coupler is conditioned, it necessarily responds in aggregate This makes it difficult to know which components dominate the behavior and limit performance As multipacting and RF conditioning are largely surface phenomena, modeling effectiveness is limited We developed a test stand to evaluate individual components of the TTF coupler design

Schematic Layout of Test Stand with Parts to be Evaluated RF load window WG to coax Device Under Test RF in

More Detailed Cross Section of the Test Fixture RF in RF out Parts to be Tests –straight 40 mm diam. coaxial line –SST and copper plating by different recipes –straight 40 mm coax with bellows –cold window assembly with window –cold window assembly without window

Specialized Vacuum WG-to-Coax Transitions Designs accommodated existing high-power vacuum windows at SLAC

UCRL-CONF Detachable Center Conductor Significant effort went into ensuring the center conductor could easily disconnect upon opening the test stand, but still maintained solid electrical and thermal contacts with the anchors on each side. This was done by screw-attaching the center- conductor length on the right, and having the center slide into a 4-jaw BeCu receiver on the left.

Test Stand Set Up WR650 vacuum window custom waveguide-to- coaxial transitions coaxial step transitions from 62 to 40 mm straight coax Device Under Test electron pickup probe The coupler component test stand at SLAC can test components up to 5 MW at 1.3 GHz at pulse lengths up to 1 msec.

Artist View of our Setup (Viewed Through Plastic Screen)

Plot Showing Vacuum Activity Consistent with Expected Multipacting Bands for a Straight Coax While observed bands generally agreed with simulations, there were difference in the power level and width. The variations are being further investigated, but are suspected to be related to either onset delays in MP emission relative to the RF wave or space charge effects, neither of which are present in the simulations.

600mm long straight SS coax section test results 600mm long straight Copper plated SS coax section test results Strong MP around 300kW!

Magic Simulations Secondary electron energy: is the work function of material (4.31 for Fe and 4.98 for Cu) The peak of secondary electron is at 24 cm coax line, OD 40mm, ID 12.5mm, 1.3 GHz RF, TW [a,d] SEY based on the measurements [b c] scaled to better match data Simulation results depends on the Secondary electron distribution Red for Copper and blue for SS

MAGIC Multipacting Simulation and ‘Resonant Finder’ Results for a 40 mm Coax Line

The electron signal turn-on time is unstable after initial processing, likely due to insufficient electrons available to seed the onset of multipacting.[1] [1] D. Raboso, A. Woode, “A new method of electron seeding used for accurate testing of multipactor transients”, Vol.1, Oct Behavior of the Electron Pickup Signal E-signal RF.

[a] The RF pulse with a 1us high power (3MW) spike; [b] The multipacting electron signal [a] 1 Time: ns Forward RF power level normalized to 300kW Electron signal amplitude normalized to 30mV [b] [a] 200ns RF pulse Spike [b] Multipacting electron signal. Multipactor Seeding and Time Response

Harmonics of the Electron Probe Signal Reconstructed electron signal Signal Recorded with 5 GHz Scope

TTF3 Coupler Multipacting Simulation Using Parallel Code Track3P Lixin Ge Advanced Computations Department SLAC

Warm Windowcold TTF3 Multipacting Simulation Components Taper Region Input Power: 0-2MW, Scan interval: 50KW.

Cold Coax 300mm 6.25mm 20mm Simulation Cases: 1. with/without reflection 2. with/without external magnetic field 3. with variable center conductor DC biases Conclusions: Our multipacting simulation results are in excellent agreement with theoretical calculations and experiment measurements at SLAC.

40 mm Diameter Coax Simulations Delta as a function of RF input power and Multipacting order

Samples of particle’s resonant trajectory Reflection: 0.4 Input power level: 160KW Order: 5th order Impact Energy region: eV Reflection: 0.8 Input power level: 580KW Order: 2nd order Impact Energy region: eV

Cold Bellows ModelMesh Cold Coax with Bellows NO multipacting activities in the bellows region Particles Distribution after 20 impacts Particles Distribution at 2 nd Period Particles Distribution at 100th Period 400 kW input power

5mm 1mm 0.4mm Ceramic Window Region Distribution of two points resonant particles’ impact energies, orders versus Input Power between the ceramic window and cold cavity Model and meshField One resonant particle’s trajectory at 0.68 MW input power 2000eV 3800eV

RF Leak Check Example of RF Processing History – See Smooth Ramp-Up in Power (Slight Dwell at 300 kW)

Similar Results at DESY/Orsay - D. Kostin, XFEL EIFast XFEL mtg 2006

Overall Summary Predicted MP is not always observed due to smearing effects, especially for high order resonances Due to absorbed gases on WG surfaces, SEY initally high, producing noticeable MP – however it diminishes as gas is removed from electron/rf interactions TTF3 coupler shows no noticeable MP ‘barriers’ during processing.