1 EuroTeV High Bandwidth Wall Current Monitor Alessandro D’Elia AB-BI-PI.

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Presentation transcript:

1 EuroTeV High Bandwidth Wall Current Monitor Alessandro D’Elia AB-BI-PI

2 Wall Current Monitors Wall Current Monitors (WCM) are commonly used to observe the time profile and spectra of a particle beam by detecting its image current.

3 The 3 rd generation of CLIC Test Facility (CTF3) foresees a beam formed by bunches separated of  b = 67 ps WCM h. f. cut-off = 20 GHz for a total pulse duration of  r = 1.54  s WCM l. f. cut-off = 100 kHz The “initial” aim Bake out temperature:150 C Operating temperature:20 C Vacuum:10 -9 Torr 100kHz-20GHz WB signal transmission over 10-20m. Furthermore

4 The gap resonances With the courtesy of Tom Kroyer (“A Structure for a Wide Band Wall Current Monitor”, AB-Note RF)

5 A more accurate study of the gap resonances The resonances due to the cross section changing are “structural”!!!! You cannot delete them, you can only to try to reduce them! TM01 cut-off  6.9GHz TM01 cut-off  24GHz The TM01, with the frequency of about 6.9GHz will be trapped between the two coaxial

6 Feedthrough resonances When the distance between two feedthroughs becomes equal to the free space wavelength, the first azimuthal resonance appears in the structure With the courtesy of Tom Kroyer (“A Structure for a Wide Band Wall Current Monitor”, AB-Note RF) With n =4, one has F =8.3 GHz

7 The whole structure With the courtesy of Tom Kroyer (“A Structure for a Wide Band Wall Current Monitor”, AB-Note RF) Therefore to have 16 feedthroughs means to push the previous resonance to  33 GHz

8 The effect of feedthrough’s on the TM01 resonance In the transversal plane you have either for vertical or horizontal directions that

9 The effect of feedthrough’s In order to reduce this enhancement, would have to happen that the distance between two feedthrough’s should be at least equal to one half of the resonant mode wavelength Indeed for a structure having andThe optimum is for n=6

10 Some consideration The two requirements concerning the feedthrough resonances and the effect of the feedthrough enhancement on the gap resonances are in conflict: Feedthrough resonancesGap resonance enhancement d h has to be, on the one hand, as small as possible, on the other hand, at least equal to one half of the TM01 wavelength

11 Three possible solutions found The last two structures present an aperture reduction of 15% and 30%, respectively. For that reason the first one has been chosen.

12 The chosen structure Silicon Carbide (tang  = 0.3,  r = 30 )

13 Some geometrical details

14 S-parameters

15

16 Longitudinal coupling impedance: Real part Longitudinal coupling impedance: Imaginary part

17 The real structure (1)

18 The real structure (2) With the courtesy of Vincent Maire

19 Transmission at the feedthrough

20 Longitudinal coupling impedance: Real part Longitudinal coupling impedance: Imaginary part

21 With the courtesy of Vincent Maire Feedthrough positioning (1)

22 Feedthrough positioning (2) With the courtesy of Vincent Maire

23 Misalignement problems With the courtesy of Vincent Maire

24 Really do we need 100kHz low freq cut-off? Let’s make some numerical experiment Bunch separation = 83ps RMS bunch length = 13.3ps Train duration = 8.3ns Nb of bunches = 100 Peak current = 293A 83 ps

25 Let’s apply a perfect low pass filter

26 83 ps The result in time domain

27 Let’s apply, to the same signal as before, a filter having Low freq cut-off= 5GHz High freq cut-off= 20GHz

28 83 ps It seems that nothing changes!!!!

29 An interesting exercise Same condition of before, but some bunches are missed (about 50%)

30 Because of the different, larger, bunch spacing, in the spectrum some new peaks appear at lower frequencies Perfect 100 bunches spectrum

31 Wrong signal recovering!!! Correct signal recovering!!! Original signal

32 Some consideration If some bunches are missed, we need a proper low frequency cut-off in order to solve the larger bunch spacing appearing in the spectrum like new peaks at lower frequencies. Therefore the low frequency cut-off should be settled up in relation to the maximum expected missed bunch ratio.

33 Applying the WCM “real” signal Low freq cut-off  2GHz 500 ps  6 bunches missed (Or 30 by compensating down to 400 MHz)

34 83 ps The result in time domain

35 A last academic exercise RMS bunch length = 13.3ps Train duration = 2.5ns Nb of bunches = 23 Peak current = 293A Just to have more fun it has been added also a random noise level of about 10% with respect to the signal amplitude 83 ps 108 ps 457 ps

36

37 83 ps 457 ps 108 ps

38 Measurements on the existing design The existing design is based on a previous design for the CTF2 (63 MHz  bandwidth  10 GHz ) Beam but Bigger volume of ferrite in order to lower the l. f. cut-off to 100 kHz The miniature feedthrough modified in order to extend their bandwidth beyond 20 GHz 8 feedthroughs

39 Experimental setup and testbench

40 Old measurements (March 2006) With the courtesy of Lars Soby and Ivan Podadera Frightening results!!!!!  7GHz

41 New measurements (November 2006)  9 GHz Quite better measurements!!!!!

42 What was wrong? The experimental setup showed very bad RF contacts between WCM and the two external straight tubes. In order to improve the contacts some pasty stripes of conducting material has been used…. Unfortunately it cannot be used in vacuum…. For frequencies higher than 12 GHz strong reflections occur because of the adapting cone are not enough smoothed. Bad RF contacts!!!

GHZ With the courtesy of Raquel Fandos

44 By making the transitions longer the resonances get less dramatic L=200mm With the courtesy of Raquel Fandos

45 Conclusions and outlooks WCM specifications has been reviewed in a more critical way, showing less stringent constraints The e-m design is accomplished, giving pretty good results At the end of the next week the mechanical designs will be sent to the mechanical workshop to start the machining and the assembling The testbench has been improved On December the first measurements and the characterization are foreseen