30kA Energy Extraction Semi-Conductor Switch SM18 - CLUSTER D Recall Gert Jan Coelingh on behalf of all team members TE-MPE-EE.

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Presentation transcript:

30kA Energy Extraction Semi-Conductor Switch SM18 - CLUSTER D Recall Gert Jan Coelingh on behalf of all team members TE-MPE-EE

OUTLINE Project team SM18 Requirements / Functional Specification Schematics / Design Criteria Topology Simulations Status To do Conclusion

Project team Core team members: Gert Jan, Alexandr, Arend, Mateusz Supporting teams electronics: Bozhidar, Pål, Szymon, (Ron) Supporting team 1 electro-mechanics: Mathieu, Samuel Supporting team 2 electro-mechanics: Stephen, Grzegorz, Krzysztof Others involved: Knud, Future TS, Solomon (ext): 2D-, 3D- & production drawings Mathieu: production drawings

Building 2173 aka SM18 - Cluster D Courtesy PERRET Ph.

Requirements EE Cluster D Demand coming from MSC group (SM18) for Energy Extraction Systems: Fast opening time (< 2 ms) High Current 30 kADC Medium Energy (10 MJ) Maximum extraction voltage: 1000V Fast opening time means; can’t be achieved with Electro- Mechanical Breakers Alternative: Semi-Conductors Chosen type: Integrated Gate Bipolar Transistor (IGBT)

Requirements F.S. TYPICAL MAGNET PARAMETERS Maximum stored energy : 10 MJ Short Sample current : 21.5 kA Magnet inductance ( ex. Of HL LHC QXF type) : mH/m Magnet length : 1 – 4.2 m max. Nominal Ramp Rate: 11 – 20 A/s Maximum Ramp Rate: 200 A/s

Requirements F.S ENERGY EXTRACTION OF CLUSTER D The energy extraction will be made with and external dump resistor. The dump resistor value will be adjusted case by case and in function of the necessity but always set such that with the maximum expected quench current the voltage stays below the last successfully qualified test value, typically obtained during a test performed while the whole magnet is in LHe and ready for the test. The max. value is 1000 V. To extract the maximum energy and stay within a given voltage, lower than the designed value, there is a strong interest to place the ground of the converter in the middle of the dump resistor. The extraction will be triggered by the quench detectors with or without delays and trough a dedicated switch the power converter will be switched off and the current will go trough a free wheel. The reaction time of the switch was set up in function of the maximum allowed temperature in the most critical magnets after a quench and is set in the range below 1 ms leading to the choice of IGBT based technology EXTRACTION SWITCH OF CLUSTER D The switch will be composed by a transistor based semi-conductors of type IGBT. Two identical switches of 15 kA will each consist of 8 elements in parallel and both racks will be located in the Cluster D area under the platform. Each rack is again split up in two modules, rated for 7.5 kA. One IGBT will carry a maximum of A depending on number of elements in parallel. The current sharing is expected to be better than 5% difference between the individual IGBTs, leading to temporary maximum currents of 1970 A for short durations (minutes). The maximum forward voltage of each switch will be 3 V. Therefore no redundancy in the system will be possible so this switch will be directly acting on the circuit. The command chain will be doubled as far as possible to guaranty the opening of the switch. It will be mono polar and the reaction time (time from FPA to 0 current in the switch) will be less than 1 ms. To be remarked that the max. of 1000 V will be also seen by the switch in blocking mode. The maximum forward losses, roughly 30 kA x 3 V will be 90 kW and water-cooling is needed. At the time of writing this document a flow rate is estimated at 200 l/min. This may decrease since the forward losses are linear with the circuit current and a higher delta T of the water in vs out may be accepted at occasions where 30 kA is needed. The estimated floor space needed for each of the two switches will be maximum 2 x 1 meters with a maximum height of 2.20 meters. There will be free space of 1 m around each of the switches allowing access to it. Each 15 kA switch will be connected, by means of a 2x2x200mm2 ultra-low-inductance cable to a separate dump resistor capable of absorbing 5 MJ each grounded via their midpoint THE DUMP RESISTOR OF THE CLUSTER D The resistor racks will be located at the first floor as close as possible above the switches. The total modular resistor can be changed roughly between 3.6 and 120 mΩ. The number of steps in between these values is still to be decided as well as absorbed energy for each resistor value. For each 15 kA switch, a proposal of 6 elements of 40 mΩ and 1 MJ each seems to be a realistic option. Each element will have a mid-point grounding tab. This allows 4 configurations with full energy dump.

Simplified 30 kA schematic

Simplified 15 kA schematic

SM18 Cluster D Courtesy PERRET Ph.

Design criteria 1 Reliability of the Semi Conductor Major failure causes due to Thermal design (DC application) Over-voltages due to stray inductances Over-current Forward losses reduced because of over-rating Commercial Availability

Design criteria 2 Lifetime Reliability Due to thermal cycling the lifetime decreases drastically Keep Delta T of junction < 80 ° Tj < 110°C See plot lifetime cycles

Design criteria 3 Transient processes lead to high voltage spikes and potential over-currents through single IGBT Stray inductance to be kept as low as possible non compensated stray inductance will lead to high voltage spikes Need for fully symmetrical design Trade-off: efficient cooling, current distribution & stray inductance Fully compensated design Need for multi-level snubber compensation Simultaneous switching of all 16 IGBTs (sub µs range)

15kA Switch topology TRIPLET MAIN BUS-BARS to minimise stray fields

15kA Switch schematic

IGBT: Infineon FZ3600R17HP4_B2 – the best available on the market Vce_max = 1700V, Inom = 3600A With I = 1875A (max possible current): Vces =1.6V => Junction heat dissipation ~3000W per module Junction temperature ~ °C 300 W dissipation for the terminals _B2 version comes with AlSiC base plate adjusted to thermal expension of silicon and ceramics leading to longer lifetime due to thermal cycles Main components

Design topology

Driver Emitter / Collector water cooled laminated busbars LEM Fuse flexibles distribution busbars Design topology

Laminated busbars with flexibles and Water cooling of the IGBT terminals

Design topology Triplet main busbars equipped with one branch, including fuse, LEM and shunt resistor

IGBT cooling plates Thermal calculations

IGBT cooling plates

Complete power cycle (charge, discharge) Power simulation

Two 15kA systems - opening details with the different synchronisation conditions Power simulation

Delay: 1ms Power simulation 200us/div Green – switch #2 current (that one which delayed to open) Cyan – switch #1 current (that one which opened) Blue and black – currents through the snubber capacitors 0, A 15k A

Power simulation Green – switch #2 current (that one which delayed to open) Cyan – switch #1 current (that one which opened) Blue and black – currents through the snubber capacitors Delay < 1µs 200µs/div 0, A 15k A

One 15kA system - opening details with all parasitical and protection elements taken into account Power simulation

Black – current trough the one IGBT Green – Voltage over one single IGBT Cyan – snubber capacitor current Red – dump resistor current Power simulation 200µs/div 1040 V 1875 A 0 A, 0 V 15k A 0 A 1875 A

The Project Today

Progress for 7.5 kA Prototype IGBTs on the heatsinks Laminated busbar (emmiter) Laminated busbars (collector + emmiter) with the IGBT

Progress for 7.5 kA Prototype DC IN DC OUT Rack assembling

Advancement for 7.5 kA Prototype mounted First type tests on-going Water pressure test – 25 bars – 45 minutes – completed and ok Insulation test – 2.5 kV vs gnd – completed and ok More while we speak

Progress for 7.5 kA Prototype Thermal studies Printing the grease trough the stencilGrease pattern on the IGBT after printing Stencils with the thickness from 60um till 120um were tried, after the pattern analysis the 80um was chosen

Progress for 7.5 kA Prototype Test stand for the thermal studies With the “normal” IGBT With the “open” IGBT

Progress for 7.5 kA Prototype Homemade heatsink Mersen heatsink Thermal studies, heatsinks (cooling plates) Infineon KW51 heatsink

Progress for 7.5 kA Prototype Thermal studies conducted by Alexandr and Bozhidar: Report almost available for distribution: Conclusions Three different heatsinks were tested All three heatsinks have the similar efficiency (difference < 1 %). “Home-made” heatsink: Pro: compatible to the existing topology which is however complex Pro: likely to be cheaper (50%) Pro: could be improved but is not needed Con: need specialist and time for IGBT mounting “Mersen” heatsink: Con: not mechanically compatible Con: guaranteed by manufacturer to 10 bars Con: need specialists for IGBT mounting “Infineon” heatsink: Con: needs water-connection adaption Pro: could be delivered with IGBT mounted BUT – chosen topology is correct, grease interface is correct, results in the all cases are excellent, theoretical calculations are confirmed by the measurements!

Progress for Dump-Resistor

Switch-Protection The EE system protects the s.c. magnet Maximum allowed forward voltage: 1700V (including spikes) Maximum circuit current: 30 kA Modular Extraction Resistance from 3.5 – 120 mΩ Possible extraction voltage maximum: 3600V (+/ to ground without ground fault) Extraction Resistor measurement with preventive/corrective action Limit power converter current (preventive) External source needed to measure total resistance value and values to ground Details to be decided. Study conducted by Szymon

To do Priority 1, 2 and 3: Prototyping.. Still to be solved: Many details… see next presentations Electronics Software External communication QA Documentation

Conclusion  Many technical details need to be addressed and solved  Probability to succeed within proposed planning is extremely small LHC operation has absolute priority Availability of 2 of the core members is not enough PJAS core member (with 15 years of IGBT experience) will leave