MQXFS Coil V1 Fabrication Status -Winding and Curing Miao Yu 2015-05-12.

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Presentation transcript:

MQXFS Coil V1 Fabrication Status -Winding and Curing Miao Yu

Coil fabrication status 2 MQXFS Coil 01 MQXFS Coil 03&05MQXFS Coil 02MQXFS Coil 04&06 LARP have wound and cured 6 coils at FNAL R&I at BNL Cut and inspected R&I at FNAL Being tested in a Mirror structure R&I at BNL Shipped to BNL for magnet assembly Coil 04 prep. for I at LBNL Coil 06 prep. for I at FNAL Both will be ready in June

Winding 3 Winding tension: 9 kg for 1 st turn, and then increase to 25 kg Wind the coil with the tool and the binder (No popped strands, observed from coil 01 cross-section) End parts fit before/after curing

Curing Apply 90 grams Ceramic Matrix Binder (CTD-1202X) to L1, and 120 grams to L2. (~0.5 gram per meter of cable) 4 L1 Curing L2 Curing

Main Issue and Solution Coil 01, 02 & 03-L1: Oil like fluid contaminate the insulation, found after curing. Cause: The laser sintered part is porous and machine oil can be trapped during slits cut, leaking out during curing. Solution: Clean the parts before coating (alcohol soak and ultrasonic in water.) Coil 03: 1. Cable Reverse bending Cause: not carefully verify the cable orientation on the spool and swapped L1 spool and L2 spool. Solution: detail description in the traveler to prepare the cable. 2. Insulation damage Cause: Install L1 LE saddle without removing the connecting screws to the splice block. The saddle was not flexible and cut the insulation during installation. The cable looked OK under magnifier. Solution: read through each step in the traveler. 5 Coil 03

Main Issue and Solution (Cont.) Coil 04: L1 LE and RE spacers were swapped, so L1 shifted toward LE by ~10 mm. Cause: After coating, the identification becomes fuzzy. Solution: All the parts go through QC carefully and highlight the ID using red marker. Coil 05: No main issue. Coil 06: Plasma coating came off the L2 Splice block Cause: G10 shim was 1 mm thicker than nominal 3.8 mm, so over compress Nb 3 Sn lead during curing. During winding, we measure the step size between the saddle and the splice block (usually larger than the nominal due to the flexible saddle). Solution: Use the nominal size shim 6 Coil 04 Coil 06 Coil 02Coil 03Coil 04Coil 05Coil 06 L L

Pole Gap Due to winding tension and thermal contraction during reaction, pole gap is required to release the strain energy. After reaction, the target for the pole gap is 0. 7

Summary 6 MQXF short coils have been wound and cured. Tooling for winding and curing were checked. Coil parts were check and fit well in the coil. Coil 03 insulation damaged during winding, and the cable should be OK. Coil 04 has 10 mm shift between L1 and L2 due to parts swap. Coil 05 have no major issue in winding and curing Coil 06 over compress the L2 lead during curing 8