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Published byJeffery Stevens Modified over 8 years ago
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Calorimetric Power Measurements in Xbox-1 Xiaowei Wu
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Preface What? Measure the extraction power after the structure Why? Cross check with the directional coupler Complement directional coupler results How? Use flowmeters and temperature sensors to build 22calorimeter
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Outline Introduction to Xbox-1 and calorimeter system HFSS and ANSYS simulation of the load Experiment results and analysis Conclusion and future work
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Outline Introduction to Xbox-1 and calorimeter system HFSS and ANSYS simulation of the load Experiment results and analysis Conclusion and future work
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Xbox-1 Layout Clockwise from top-left: Modulator/klystron (50MW, 1.5us pulse) Pulse compressor (250ns, ratio 2.8) DUT + connections Acc. structure Bunker Gallery B.Woolley, “High-gradient testing in Xbox-1”, CLIC workshop 2014, Geneva, Switzerland
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Concept of the Calorimeter
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Outline Introduction to Xbox-1 and calorimeter system HFSS and ANSYS simulation of the load Experiment results and analysis Conclusion and future work
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Review of the SS430 Load Cross Section of ¼ load Model of ¼ load Water outlet Water inlet Power input
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Review of the SS430 Load 93.8 WG taper Matching section Regular part 265 WR90 5.0 Total 892 End cup 30.5 488 Material information: SS430: σ =1115384 S/m, μ =6 Regular part: 50dB/m loss Regular part’s cross section S.Matsumoto et.al., “High power evaluation of X-band high power loads”, LINAC10, Tsukuba, Japan
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Electromagnetic Simulation for the Load
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Thermal Simulation for the Load HFSS and ANSYS coupling simulation Electromagnetic field simulation in HFSS Export surface loss results into ANSYS workbench Use Steady-state thermal analysis module to calculate the heat distribution of the load ANSYS workbench panel
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Convection Calculation for the Flow From fluid dynamics knowledge… Re and Pr are known for fixed flow in pipe
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ANSYS Simulation Results 117W for ¼ load with 11.9L/min, 25 degree flow Matching part is hottest! Temperature along the welding joint line
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Outline Introduction to Xbox-1 and calorimeter system HFSS and ANSYS simulation of the load Experiment results and analysis Conclusion and future work
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Setup for the Calorimeter System Calorimetric measurement was done in new CPI klystron’s commissioning Time: 2014.5.21~2014.6.23 Output peak power reached almost 23MW, pulse width 1us Schematic diagram of the Calorimeter Load tree two X-band high power loads Flowmeter SMC-PF3W720F04ETM
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Xbox-1 Layout Modulator/klystron (50MW, 1.5us pulse) Pulse compressor (250ns, ratio 2.8) DUT + connections Acc. structure Bunker Gallery
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Calorimetric Measurement Lay-out Xbox-1 Modulator & KlystronLoad “Tree” Modulator/CPI new klystron Load Tree + connections
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Full History of Calorimetric Measurement Data from 2014.6.18.16h~2014.6.23.08h Directional Coupler Measurement Calorimetric Measurement Peak pulse power 14MW~22.6MW Pulse width 942ns Flow rate 11.9L/min
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Full History of Calorimetric Measurement Average power comparison Directional coupler ~ peak power*pulse width*repetition rate Calorimeter ~ specific heat*flowrate*temperature difference
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0619-08h~0619-16h, 8 hours’ data Seems not very good at the beginning… 15% difference compared with directional coupler’ results
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0620-08h~0620-16h, 8 hours’ data Becomes better when input power becomes more stable ~10% difference compared with directional coupler’s results
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0621-08h~0621-16h, 8 hours’ data Difference decreases to less than 7% when input power is stable
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0622-00h~0622-08h, 8 hours’ data Calorimetric results fit with directional coupler’s results in steady state Less than 7% difference between the two results Less than 7%!
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0622-08h~0622-16h, 8 hours’ data Calorimetric results fit with directional coupler’s results in steady state Less than 7% difference between the two results Less than 7%!
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More Analysis about the Results Time delay is observed when power ramping up again due to the breakdown In average power of 938W with flow rate of 11.9L/min, time delay is about 50 seconds Cause big difference compared with directional coupler results 50s
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Temperature Distribution Measurement Add temperature sensors along the welding joint line Five sensors on each load 938W average power with 11.9L/min flow Experimental result fits well with ANSYS simulation!
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Error Analysis Flowmeter’s error~3% accuracy, 2% repeatability(can be serious…) Heat insulator is not perfect (caused heat leakage) Power lost in the transportation system (waveguide/splitter…) Same flow, but different display in flow rate and temperature Energy loss Splitter temp is a bit high
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Outline Introduction to Xbox-1 and calorimeter system HFSS and ANSYS simulation of the load Experiment results and analysis Conclusion and future work
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Conclusion First calorimetric measurement in Xbox HFSS-ANSYS coupling simulation is feasible Calorimetric results fit well with electromagnetic measurements
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Future Work Redo the calorimetric measurement in Xbox-2 Flowmeter is already installed in Xbox-2, cabling work Measure the energy in different flow rate/water temperature/peak power/pulse width In our measurement, flow rate and pulse width keeps constant Make calibrations for flowmeter with known flow Increase the accuracy of flow rate’s reading Use more precise flowmeter
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Thanks for your attention!
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