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Published byJoy Stewart Modified over 8 years ago
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Group 5
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History Structure Failure Scenario Reasons of Failure Engineering Mistakes
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Built in 1973 in Kansas City Multipurpose Stadium Ice shows, conferences, basketball, soccer games... Capacity of 17,000 Contemporary Design Received an award in 1976 from AIA Cost $23.3 million to build
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25m 100m 95m Steel trusses hung from three portals Steel trusses supported RC roof
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4 th June 1979 One in ten year storm ○ 120 km/h winds ○ 10 cm of rain per hour Roof collapsed Rapid air pressure increase blew out walls Portals remained undamaged 0 victim
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Roof used as temporary reservoir during storms Accumulation of water due to inadequate drainage Ponding of the roof Roof began to sag and more water accumulated Increase of load supported by the roof
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Bolts subjected to high rate of oscillations since erection of Arena Fatigue of Bolts Bolts failed in one hanger due to load increase on the roof Domino effect caused others hangers to fail
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Drainage system : ○ Use of 8 drains of diameter 12cm ○ 55 were required according to local codes What should have be done : ○ Respect of Building Standards
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Bolts : ○ Use of A490 bolts (can only maintain tensile strength for static conditions) ○ Failed at 1/3 of Design Capacity due to fatigue What should have be done : ○ Design of bolts under dynamic conditions
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Domino effect : ○ Lack of redundancy in the hangers What should have be done : ○ Better load distribution
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Group 5 Michael Harte Emma-Jane Heneghan Matthieu Huot Kiara Ryan Angharad Sweeney Thank You!
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