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Effective Strategies for Industrial Energy Efficiency: Opportunity Identification and Implementation
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Effective Strategies for Industrial Energy Efficiency
Energy Efficiency through Industry and Process Specific Technical Assistance MnTAP Intern Program: Achieving Results Today while Preparing for Tomorrow Researching New Industrial Energy Efficiency Strategies and Opportunities
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Minnesota Technical Assistance Program
Created in 1984 Located at the University of Minnesota Provide pollution prevention, waste management, water conservation and energy efficiency assistance Confidential and Non-regulatory
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MnTAP Mission Strengthening Minnesota businesses by improving efficiency, while saving money through energy, water and waste reduction. Businesses remain competitive Improve employee and public health Protect the environment
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Industrial Process Assistance
Pollution prevention More efficient use of raw materials Water conservation strategies Energy efficiency opportunities Cost savings for businesses!!
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Energy Efficiency Assistance
Process energy focus Compressed air system audits Steam system/boiler efficiency Process heat management Motor, fan, and pump efficiency Resources Certified Energy Managers on staff Case Studies Process energy efficiency – Certified Energy Managers on staff. Many examples from site assessments, special projects and Intern projects. See MnTAP website on E2
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Project: Industrial E2 Program
U.S. Department of Energy through the MN Department of Commerce Outputs Outcomes 200 people trained 100 businesses impacted 34 sites assessed 6 intern projects 3 teams launched 130,000 MMBtu reduced 250,000 lb chemical reduced 22 million gal water reduced $1 Million yearly savings
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Trident Seafood: Implemented Results
Motley, Minnesota Participated in steam assessment training and an audit Implemented four recommendations Used most efficient boilers Recovered heat with condensing economizer Replaced inefficient equipment Repaired boiler control system Estimated Annual Savings 258,000 therms $154,000
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Project: Wastewater Treatment E2
U.S. EPA Region 5 Outputs Outcomes 10 site assessments 1 intern project 4 assessment presentations 5 technology demonstrations benchmarking 1.22 million kWh $86,000 Project Recommendations 5.56 million kWh $444,000 project Current project is : benchmarking, assessments, and CHP component (3 interns) – 2 in 2017 Long term time horizon – large investments… Bring in partners collaborative efforts now
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MnTAP Intern Program – Achieving Results while Preparing for Tomorrow
Focus on solutions for P2/E2 projects Students hired by MnTAP Extra engineer for the summer Reports direct implementation Energy projects partner with utilities Company cost-share suggested Solutions online summary of 2013 projects Summaries of 2015 projects
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Impact Energy: Lloyd’s Barbeque Company
Mendota Heights, Minnesota Manufactures: Cooked meat products Improve hot water management Install wash tank temperature regulator Optimize hot water pump pressure Results: 50,000 therms 25,000 kWh 1.3 million gal water $54,000
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Impact Energy: Caterpillar Paving Products
Manufactures: Road paving machinery Improve compressed air efficiency Optimize compressed air use Install VSD Upgrade control sequencing Find and repair leaks Repair >100 leaks Isolate equipment not in use Results: 300,000 kWh $28,000 Brooklyn Park, Minnesota
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MnTAP Intern Program Results
2016 Recommendations 3.1 million kWhs 143,000 therms 5 year Implemented Results* 11.5 Million kWh’s 1 Million therms $2.4 Million savings Students – experience in energy efficiency assistance 2016 MnTAP Interns *Verified by direct follow up with companies
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MnTAP Intern Program Success
“The outcome of the project has resulted in a minimum of 20% reduction in electrical demand of the aeration system and has created the momentum for even more reductions to occur.” ~Tracy Hodel, Assist. Public Utilities Director, City of St. Cloud WWTF “Our intern was a great candidate for a future employee. He dove head on into his process improvements with an awesome hands on approach!” ~ Lee Gulbrandson, Manufacturing Engineering Manager, Lou-Rich “Working to improve energy efficiency provided the perfect opportunity to expand my technical knowledge and analytical skills. This experience taught me how to work and communicate effectively with the variety of stakeholders involved in a large-scale manufacturing operation.” ~WB “Xcel Energy values the MnTAP Intern Program and the projects that are identified each year. The program helps us to provide extra resources to our customers who value the high quality projects they get in return.” ~Molly Hiipakka, Xcel Energy Customer Solutions The MnTAP Intern Program is considered a success by companies, utilities and students Cost effective identification of efficiency opportunities Provides interface with utility efficiency programs Measures and verifies energy efficiency implementation Provides students with industrial experience and strategies to carry energy efficiency focus into their careers
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Energy Efficiency Research
Explore new industrial efficiency approaches Industrial sector specific opportunities Benchmarking Develop tools and resources Energy use calculators Case Studies Process energy efficiency – Certified Energy Managers on staff. Many examples from site assessments, special projects and Intern projects. See MnTAP website on E2
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Motivating Manufacturing Energy Efficiency
CARD Grant Integrated energy assessments and lean manufacturing in MnTAP intern projects to provide efficiency recommendations and implementation assistance Motivating Manufacturing Energy Efficiency: E2 Assessments & GreenLeanSM Training with Directed Implementation MN Dept of Commerce Division of Energy Resources CARD Reports
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Motivating Manufacturing Energy Efficiency
Direct energy reductions Variable frequency drives Optimize process set point Motor inventories Maintenance schedules for high energy equipment Upgrade lighting Optimize compressed air traditional
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Motivating Manufacturing Energy Efficiency
Increasing Throughput Optimize work flow Streamline process set up/change over Eliminate off-specification product Achieve more production per unit energy Lean manufacturing tools / assessments to augment savings
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Project Outcomes Suggestions Recommendation Value Implemented
Reduction Savings Traditional Energy Efficiency 7 648,000 kWh $59,000 6 257,400 kWh $23,000 Lean Identified Process 11 586,800 kWh 2,200 therms 294 hr 75,000 lb $491,000 4 438,400 kWh 11,000 therms 38,000 lb $247,000 Lean Activities 29,000 kWh 2,600 therms 1,850 hrs 53,000 lb $176,000 3 24,200 kWh 800 hrs $55,000 Total 25 $726,000 13 $325,000
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Impact Energy: Uponor Corporation
Apple Valley, Minnesota Manufactures: Extruded cross-linked PE pipe Increase output with lower energy Optimize curing process Insulate extruder barrel Results: 448,000 kWh $44,000 One of 7 intern projects was:
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Power Tool Energy Efficiency Research
CARD Grant Define energy conservation potential for conversion of pneumatic to electric tools Resource development Pneumatic tool guide Conversion cost calculator Supported by a grant from the Minnesota Department of Commerce, Division of Energy Resources through the Conservation Applied Research and Development (CARD) program.
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Power Tool Energy Efficiency Research
Preliminary findings $5,000,000 per year powering tools with compressed air 85% savings opportunity with electric alternatives Electric driven tools have reasonable payback period 6 months (corded) 11 months (cordless / rechargeable) Our preliminary results suggest
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Call MnTAP For: Customized Technical Assistance Resource Conservation
Site Visits Interns Training and Resources Resource Conservation Air Emissions Water Conservation Energy Efficiency
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Thank you – Questions? Strengthening Minnesota businesses by improving efficiency, while saving money through energy, water and waste reduction. Laura Babcock Paul Pagel
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