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Recent TOB Developments
C. Campagnari On behalf of the US module testing groups
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Outline Status Update CMN (Micro-discharge) Problem
4 Hybrid Thermal Cycler Stereo and 6 chip module production Dead pipeline column fault Module Burn-in (Wien Cold Box) Status Grounding improvements Backplane pulsing First US Rod CMN (Micro-discharge) Problem Description of problem Why you should be concerned about it? Studies performed Future plans/Request for aid
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Hybrid Thermal Cycler-Pulser
Now fully commissioned at UCSB Many thanks to CERN group for their constant aid ~40 minutes to thermal cycle 4 hybrids 6 hybrids had APV-PA bonded at UCSB 4 6-chip hybrids 1 4-chip R-F hybrid 1 4-chip stereo hybrid No opens or shorts caused by bonding
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Hybrid Thermal Cycler at UCSB (2)
Scope mode (25 ns between each acquisition) Opens added to hybrid to test PA pulser Opens clearly seen in both scope mode (above) and pedestal tests (below) Should have no problems detecting problems in hybrid bonding All 4 chips shown here
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Modules Produced with Final Hybrids
First Stereo TOB module made!!! 3 TOB stereo module produced in total All well within specs mechanically and all Grade A Kapton circuit was missing a trace for bias. We made it by hand with Ag Epoxy. One chip has dead pipeline column Found to be dead prior to module production 2 TOB 6-chip R-F module produced (first module of this kind produced!!) Both Grade A 1 TOB 4-chip R-F module with final hybrid built Grade B due to known sensor faults
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Dead Pipeline Column (1)
Chip with unusual pulse shape and pinhole tests found (see next slide) After conferring with Aachen and CERN, problem appears to be confined to one pipeline column After taking a pipeline test with many events, it became clear that the noise of a pipeline column was too low to be active (Dead pipeline column) Noise is lower than APV in bare hybrid
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Dead Pipeline Column (2)
Other symptoms of dead pipeline columns Pulse Shape Test No calibration injection 0.5% of events Causes dips in pulse shapes Pinhole Test 1 in 192 chance of having no calibration injection, causing channels to be marked as pinholes Need to modify hybrid testing procedure to find dead column prior to module assembly Measuring pulse height in pipeline-like test with calibration injection would find this problem 100% of time Problem is not serious enough to cause rejection of module ~ Equivalent to dead channel
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Module Cold Box Status All functionalities demonstrated (UCR/UCSB)
Cold box fully instrumented 10 UTRI, 10 PAACB, FED multiplexer, 2nd CCU and electrometers Works with multiplexer, electrometers and PAACBs Performed long term module tests during production run with full readout of temperatures and currents Since September CMS week Implemented grounding scheme to reduce noise greatly with multiple modules Conducted first backplane pulse tests
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Module Cold Box Noise at UCSB
Before After High noise on all 8 slots tested Grounded hybrid-to-UTRI adapters to cold box plates. Noise reduced on all slots enough for defects to be seen. Both at UCSB and FNAL
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Backplane Pulse Test in Cold Box
Shorted to two channels Open (to remove short) Open Open Open (to remove short) Shorted to two channels Module 1025 noise with 100V bias Module 1025 backplane pulse response with 100V bias Channel with marginally low noise shows up clearly in backplane pulse response Successfully tested in LT version 1.15 (needed upgrade from 1.10)
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Single Rod Test Stand at UCSB
Complete set of electronic ready to test single rods Test box provides dry, dark, and electrical isolated environment Connects to Rod burn-in chiller for cooling Prototype rod with 3 biased modules tested on stand
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First Assembled Rod in US
First rod in US fully assembled Took approximately 2 hours for assembly Electrical tests have just begun
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CMN Problem 14 of 60 modules produced at UCSB exhibit large common mode noise (one chip only) All of the 14 modules have a larger bias current than expected from sensor QTC probing Extremely high noise on 1-4 channels on each module suggests all the excess current localized to these channels No obvious damage seen on these channels (visual inspection) No indication of problems seen in sensor QTC measurements At UCSB, problem always appeared at first test after bonding 1 module at FNAL developed problem during Wien box module burn-in after a full ARCS module characterization
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Why be concerned about CMN problem?
One can argue that this may not be a real problem for several reasons: It is mainly occurring at high bias voltages It causes only a small amount of Common Mode Noise (CMN) The noise is removed by CMN subtraction in the FED. In fact we see evidence that all of the above are not quite right: (see discussion below) It may be that more sophisticated CMN removal algorithms are needed and hopefully the FED is capable of running them It may be that the new ST sensors have a drastic reduction in this problem Study of 102 recently produced ST sensors sent to the US (thanks Manfred et al.) gives indication that problem is less severe in new production In addition, CMN problem developed in 1 FNAL module during burn-in Not clear how the problem will develop during operation
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CMN Turn-on Voltage
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Common Mode Subtracted Noise
25 ADC 6.5 ADC Off scale Off scale Module #: (Peak Off) Chips with CMN (micro-discharge problem) Common mode subtracted noise in blue For majority of modules with problems, the CM subtraction is imperfect. 7 of 12 have >2.0 ADC noise 3 of 12 have more than twice the usual noise
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Common Mode Subtraction Variation
Module 1010 Module 1016 Common mode subtraction results clearly vary Answer differs mode-to-mode or test-to-test Would yield varying signal efficiency/noise during data taking Not clear how this will evolve with time/radiation
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Module 705 before LT (FNAL)
After assembly module was tested (09/08) on ARCS at 400 V and graded “B” (6 faulty channels). No problems observed.
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Module 705: LT data (FNAL) Data was taken at 20°C on Sept.19 (10 days after the first test). A group of high noise channels is seen around channel 219 and increased CMN is seen in chip #2
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Module 705 after LT – I (FNAL)
Module was re-tested on ARCS on 09/23. High noise in channel #219 and high CMN is observed at 400 V. At 200 V channel #219 has only slightly higher noise than the rest of the channels 400V
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Module 705 after LT – II (FNAL)
On ARCS kept module at 400 V for 30 minutes before testing (to allow current settle down) CMN did not go away, it became even higher
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Comparison of IV curves (FNAL)
”before” measurement is taken on 09/08 on ARCS before LT “after” measurement is taken on 09/23 on ARCS after LT green curve is a measurement done using Keithley on 09/24 with 1 minute interval between steps No visual defects are observed on the sensors around noisy channel #219 At this point we can’t conclude whether the effect we observe is due to thermal cycling or if it is some other effect
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Studies to determine origin of CMN problem
3 FNAL CMN problem modules sent to Karlsruhe for irradiation studies See talk by F. Hartmann Extensive program of sensor probing and additional module IV measurement undertaken Sensors probed prior to assembly in modules Sensors with >5 mA extra current relative to sensor QTC measurement separated from others Module then assembled and bias bonded to first sensor IV measured Bias is bonded to second sensor IV remeasured Module is then fully bonded and tested
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Sensor Probing Three Sets of Sensors Probed
Old OB2 (Week to Week ) 75 Sensors Old OB1 (Week to Week ) 31 Sensors New OB2 (Week ) 97 Sensors Environmental conditions tightly controlled Temperature C RH < 30% at all times
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Results of Probing Study - UCSB (1)
22 modules produced and bonded prior to change in procedure 4 had CMN problem 6 modules produced were IV measured prior to sensor bonding, but sensors not probed 5 show greatly increased bias current prior to bonding of channels Bonding is NOT source of problem 32 modules produced with sensor probed at UCSB 5 built with sensors with increased bias current (>5 mA) 4 show CMN problem 27 built with sensors with IV matching sensor QTC measurements Only 1 shows any indication of CMN problem Only appears in ~50% of test Problem appears to originate prior to module assembly The sampling of sensors was slightly biased toward high-fault rate sensors. Almost all from old OB2 batch.
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Result of Probing Study (2)
Probed UCSB (450 V) – QTC Measurement (450 V) Sensor Group > 2 mA >5 mA >10 mA >20 mA >100 mA < -2 mA <-5 mA <-10 mA Old OB2 15% 9% 8% 5% 1% 3% Old OB1 6% 0% New OB2 2% We observed that a bias current increase of ~5 mA can cause common mode noise Rate of CMN problem consistent with percentage of old OB2 sensors this increase UCSB probing agrees much better with new OB2 sensors!!!! Produced Week of 2002 Factor of ~4 decrease in the rate of higher and lower current measurement at UCSB relative to old OB2 sensors We need to measure sensors after all processing changes were made to confirm these result ASAP!!!!
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Preliminary Conclusions (1)
The CMN problem appears to be a sensor problem It is NOT created during module assembly or bonding The cause of the problem is NOT clear No visible damage or indication of defects from sensor QTC Pre-screening sensors (measuring IV) in US appears to improve situation greatly but: We do NOT know how the problem will evolve Rate of appearance vs. time, power cycles, etc. Changes with radiation damage How problem parts will act with in sub-structures with final electronics and power supplies Can only make ~9-12 sensor IV measurements per hour at assembly centers Would need 1-2 full-time techs for this alone at peak production Doing it somewhere else would even be better While improvement in newest batch of sensors probed were seen, we cannot rule out the possibility of having a FRACTION of effectively dead chips in the TOB and outer TEC until problem is better understood
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Preliminary Conclusions (2)
We really cannot do much more to study this problem at UCSB/FNAL Hopefully we have provided enough information to Sensor Group to continue study See irradiation/probing studies by Karlsruhe Looked into studying modules with IR camera 2 private companies found in Bari and in San Diego which can study parts with their equipment and our expertise No idea of cost 2 companies identified which sell cameras-OptoMetrix and QFI Cost about $80,000 for full system Karlsruhe has partial system Need camera and IR lenses (>$30000) Hiroshima University has a system which we may use there Really need a Sensor Group contact to continue study Do not have man-power for this and other responsibilities
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