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High Power Hg Target Conceptual Design Review Hg Jet Nozzle Analysis M. W. Wendel Oak Ridge National Laboratory February 7-8, 2005
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 2 Conceptual Design Review 7-8 Feb 05 An Initial Computational Fluid Dynamic Analysis was completed. 1 cm Hg nozzle at 20 m/s 2 1.9-cm supply lines at 2.8 m/s
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 3 Conceptual Design Review 7-8 Feb 05 Only the mercury itself was modeled in the simulation. Constant pressure at outlet. 21.3 kg/s inlet. Boundary conditions No-slip walls at all other boundaries.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 4 Conceptual Design Review 7-8 Feb 05 The computational mesh consisted of 230,545 hexahedral control volumes.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 5 Conceptual Design Review 7-8 Feb 05 The computed flow shows smooth streamlines for the inlet lines and reservoir, but extreme conditions near the nozzle inlet.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 6 Conceptual Design Review 7-8 Feb 05 The computed pressures show cavitation will occur at the nozzle inlet. Computed pressure differential is 722 psi
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 7 Conceptual Design Review 7-8 Feb 05 The computed pressures are particularly low where the flow accelerates around the corners. NOZZLE FLOW TOP VIEW NOZZLE FLOW
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 8 Conceptual Design Review 7-8 Feb 05 A shorter (1/2-inch) orifice was also analyzed
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 9 Conceptual Design Review 7-8 Feb 05 Computed stream-lines are similar and the total pressure drop is just under 800 psi.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 10 Conceptual Design Review 7-8 Feb 05 Again, cavitation is predicted, although the conditions are less severe.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 11 Conceptual Design Review 7-8 Feb 05 Cavitation is highly likely because of the low pressure at the nozzle exit, and the high velocity in the nozzle. P static = P stagnation – ½ V 2 is density V is velocity If P static < P sat, then mercury will cavitate The CFD model is not conservative in predicting cavitation due to the transient aspect of the flow which is not simulated. In the SNS Target Test Facility mitered bends, CFD results showed much less severe conditions than computed here. for 20 m/s, ½ V 2 = 400 psi for 30 m/s, ½ V 2 = 900 psi
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 12 Conceptual Design Review 7-8 Feb 05 Cavitation in the nozzle is undesirable. Short nozzle lifetime Choked flow Erratic jet flow pattern Noise
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 13 Conceptual Design Review 7-8 Feb 05 Design changes can reduce or eliminate cavitation. Redesign the nozzle Rounded corners Contoured inlet Increase the chamber pressure Ultimately the nozzle design needs to be tested.
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O AK R IDGE N ATIONAL L ABORATORY U. S. D EPARTMENT OF E NERGY 14 Conceptual Design Review 7-8 Feb 05 Recommended Future Work Analyses on improved nozzle designs Literature searches on intake nozzle designs
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