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Terumo Cardiovascular Systems: Oxygenator Production Improvement

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Presentation on theme: "Terumo Cardiovascular Systems: Oxygenator Production Improvement"— Presentation transcript:

1 Terumo Cardiovascular Systems: Oxygenator Production Improvement
University of Delaware’s Senior Design Team: Tom Craig Mike Giuliano Ronit Lilu Chase Ross Kate Staley

2 Description of Project
Project Goals: Improve the efficiency of Reservoir Assembly production line via reduction in downtime, change over time, and cycle time. Employ lean manufacturing techniques from the ground up such as participation in a Kaizen event

3 Assembly Line Reservoir Inspection Lid Assembly VR Station CR Station
Leak Tester VR CR Lid Final Assembly Lid Line Jig

4 Current Floor Layout vs. Future Floor Layout
Reservoir Assembly Table CR VR Lid Line Assembly Table Product Flow

5 Lean Manufacturing Techniques
The Kaizen event: Attended a meeting with representation from operators, manufacturing, production supervisors, engineering, and plant leadership to discuss improvements Time study Spaghetti diagrams Value Stream Mapping (VSM) Value Added, Non-Value Added Time

6 Customers & Wants Customers: Terumo Management, Terumo’s Floor Staff, Surgeons, Hospitals, Patients

7 Metrics and Target Values
Accuracy of Manufacturing/Error Proof 100% Harmful Factors 3 feet egress clearance, limit body rotation/twisting/reaching, adjustable table heights for ergonomics Minimize Space VR Table 3 ft or less, CR Table 2’ x 2’ Waste of Time less than 20%, less than 1 mile/day walking Cycle Time reduce by 4 sec (from 42 sec to 38) Productivity Increase of 675 units of oxygenators/week Risk Score below 25 RPN (no mitigating action required)

8 Current Floor Layout vs. Future Floor Layout
Product Flow Reservoir Assembly Table 1 Pass of 3 Steps 6 Passes of 3 Steps Each CR VR Lid Line Assembly Table VR walking distance/day ≈ 6.6 miles CR walking distance/day ≈ 1.5 miles VR walking distance/day ≈ .5 miles CR walking distance/day ≈ 0.3 miles

9 VR: Current State vs. Future
Future State Time Saved: mostly due to table redesign and offline production Walking Time seconds

10 VR Concepts Rotate lid assembly table and align it with Chemical Table
Redesign Chemical Table and “L” it with the assembly line Design and manufacture additional jig Take wings off jigs on table Sensors on bins to force order Reduce the 6.6 miles operator walks per day to about ½ mile (ergonomics, waste of time) Removes full rotation movements (ergonomics, harmful factors, waste of time) Cuts down cycle time to 32 seconds from 42 seconds (productivity, cycle time) Sensors to reduce/eliminate chance of error (accuracy, reliability) Establishes a better flow (waste of time, accessibility) Reduces change over time (waste of time, productivity)

11 CR: Current State vs. Future State
Time Saved: 9.9 seconds reduced time through elimination of walking (moving caps) and addition of the chemical sensor. Note: Increased VA time due to addition of inspection tasks

12 CR Concepts Move caps down to reservoir inspection
Time sensor for chemical dipping Move CR cart closer to operator Increase inspection duties Eliminates walking down the line to the caps (waste of time, productivity, cycle time) Reduces chemical dip time via a sensor system (accuracy, waste of time, reliability) Pulls CRs faster (waste of time) Aids in line balancing (cycle time)

13 Reservoir Inspection: Current State vs. Future State
Decreases walking time for CR (productivity, waste of time) Effectively utilizes line balancing concepts Reduction in Inspection Duties Line Balancing: Additional responsibilities (placement of 6 more caps)

14 Proposed Floor Layout Table at CR Station Table at VR Station

15 Final VR Table Tricots Drainage cages Fume hood Small tubes
Large tubes Small tubes Jig Position forcing tray

16 Preparation before Implementing
Risk Analysis Met with a team of Terumo associates including engineering, upper management, quality manager, and manufacturing associates to assess risk via a Terumo Risk Analysis template. Given GREEN light to go ahead Update Standard Operating Procedures Drafted changes to the SOP via text and pictures which was then reviewed and approved by Terumo

17 Implementation/Testing
Off-line implementation Operator at Terumo tested the new set-up of VR table on manufacturing floor to make sure everything easy to reach and functions well. Jig fit the lid Ergonomics were ideal – little walking and did not have to reach far Table took up smaller space Eliminated waste of time Minimal complexity and high convenience of use (operators were pleased) Acceptable risk from Risk Analysis

18 Implementation/Testing
Parts were loaded into bins to test how much they hold. Improvements: Tricot and drainage cage bin sizes increased to increase capacity Positioning adjustments made Parts in bins Current Future Large Tubes 60 110 Small Tubes 80 160 Drainage Cages 45 28 Tricots 100

19 Performance Metrics Metrics Target Values Actual Value
Accuracy of Manufacturing/Error Proof 100% Determined in Path Forward Harmful Factors 3 feet egress clearance, limit body rotation/twisting/reaching 3 ft. egress clearance met, eliminated rotations/twisting/reaching Minimize Space VR Table 3 ft or less, CR Table 2’ x 2’ VR Table 3’x 2.5’, CR Table 2’ x 2’ Waste of Time less than 20%, less than 1 mile/day walking VR = 0.5 miles/day CR= 0.3 miles/day, less than 20% waste achieved Cycle Time reduce by 4 sec (from 42 sec to 38) Cycle Time in Path Forward expected to meet 38 sec requirement Productivity Increase of 675 units of oxygenators/week 675 units of oxygenators/week expected to be met in Path Forward Risk Score below 25 RPN (no mitigating action required) Risk slightly increased but significantly under 25

20 Path Forward Terumo will manufacture the new bins for the increased capacity and new arrangement. Design can then be implemented on the line. Additional time studies and spaghetti diagrams are recommended once implemented on the line. Sensors will be implemented at a later date by Terumo. Time data Wasted time Cycle time Productivity New spaghetti diagrams Record any body rotations/twisting, quality improvements

21 Project Cost Item/Material Cost
CR Table $411 VR Table $468 Jig (block of Delrin) $262 Sensors (2 sets) $2,000 (about $1,000 each) Plexiglas (for VR Chemical Hood and VR bins – includes duplicates of bins) $400 Machine Shop- stainless steel plate $220 Total $3761 Note: Terumo will use their own Machine Shop to manufacture the jig and VR Chemical Hood. Team will use UD Machine Shop to manufacture bins.

22 $11,238,480 net gain/year Revenue Analysis 15 additional units/hour
30,960 additional units/year $12,384,000 additional revenue/year $1,145,520 additional material cost/year $11,238,480 net gain/year

23 Project Summary Lean manufacturing techniques such as VSM used to increase efficiency of manufacturing process Improved ergonomics for operators Maximized space used Decreased cycle time $11.2 million net gain/year

24 Questions?


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