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1 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Review of CMN Problem/Studies Ariella requested me to review the current understanding of the.

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Presentation on theme: "1 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Review of CMN Problem/Studies Ariella requested me to review the current understanding of the."— Presentation transcript:

1 1 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Review of CMN Problem/Studies Ariella requested me to review the current understanding of the CMN problem  What are the symptoms  What studies have been done  What we think the most likely source of the problem is Also discuss test results of the problem modules test in the current ARCS/LT analysis software  How/will the software flag the CMN problem modules  Will the software be able to find all of these problems prior to installation in rods/CMS

2 2 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Symptoms of CMN Problem A channel develops an extremely high noise When the channel’s noise is higher than 20-25 ADC, the entire chip begins to oscillate  Common mode noise seen, which is not always correctly subtracted  At this point, excess bias current always seen As low as 0.5  A excess has been seen to cause the problem Excess current needed to start an oscillation has varied between 0.5-5  A Consistent with micro-discharge; dependent on frequency of current spectra of discharge  Problem has (almost) always occurs on first test during voltage ramp up 1 module at FNAL developed problem during module burn-in with no sign of problems on effected channel  Increased bias current (almost) always seen in IV reprobing 1 module at UCSB developed high current after assembly Rules out module production and assembly as cause of problem  The voltage at which the problem begins has had a wide distribution Between 50-450 ADC No obvious visible damage seen on channels On three modules probed at Karlsruhe, the bulk of the excess current seen on channel with the increased noise

3 3 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Current CMN Status 15 of 73 modules produced at UCSB have CMN problem Once notified of problem, FNAL found 6 of 15 previously tested module also had CMN problem  In addition, 1 module developed problem during module LT testing 1 TEC module module tested at Karlsruhe also found to have problem 2 test beam modules also shown to have CMN problem  See L. Borrello’s talk in sensor meeting  1 of 6 ceramic hybrid modules in test beam  1 of 6 flex hybrid modules in test beam Both built and test prior to knowledge of problem

4 4 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN Turn-on Voltage

5 5 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN problem vs. voltage Once, IV diverges from QTC expections, noise on channel increases rapidly causing CMN at 20-60 V above the divergence point IN NO CASE WAS THERE AN INDICATION OF NOISE BELOW THE DIVERGENCE POINT OR IN QTC PROBING

6 6 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Are the faults caused by assembly? Extensive program of sensor re-probing and additional module IV measurement undertaken  Sensors probed prior to assembly in modules Sensors with >5  A extra current relative to sensor QTC measurement separated from others  Module then assembled and bias bonded to first sensor IV measured  Bias is bonded to second sensor IV re-measured  Module is then fully bonded and tested During all measurements, environment controlled  Temperature between 23-24 C  RH <30%

7 7 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 IV Correlation with CMN problems Significant differences from QTC sensor probing have been found  ~7% of sensors have current increases >5  A from QTC prior to module assembly Roughly consistent with the rate of occurrence of the CMN problem (aka micro-discharge) observed at various production sites The increased current occurs during ramp up during IV probing Production Results with IV Pre-Screening  Of the 39 modules produced with sensors whose IV curves in the QTC database matched those obtained in UCSB re-probing, only 1 showed any change in current This module showed regular current in some tests afterwards so the problem appears to be intermittent Another showed CMN problem with only 0.5  A extra bias current  Of the 5 modules with sensors whose IV curves in the QTC database with 5 extra  A of current from those obtained in UCSB re-probing, 4 had serious CMN problems Rules out hypothesis that problems due to mishandling in US Indicates any change in IV curve relative to original QTC measured a good predictor for sensors that will cause this problem

8 8 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 IV Re-Probing Pisa, Perugia, UCSB, FNAL and UR all have begun extensive re-probing program  See sensor meeting  Plan on re-probing all sensors not in modules yet 6-8% of sensors re-measured from 2001- 2002 at all four sites have a 5  A increase in current Most modules built with these sensors will have CMN problems  If we had not re-probed, we would have 10-20% modules with this problem now  We have NO understanding of the cause of the change in the bias current We DO NOT know the time constant/rate for the development of increased Therefore, we do not know if more sensors would develop higher currents once built into modules, rods, detectorTherefore, we do not know if more sensors would develop higher currents once built into modules, rods, detector FNAL PISA

9 9 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN vs Batch Sensors which cause CMN are fairly evenly distributed throughout production years 2001-2002 Early indications are that 2003 may be better  Extremely low statistics  Only low bias current sensors used

10 10 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Common Mode Subtracted Noise (Peak Off) 25 ADC 869 881 1010 1011 1013 1014 1015 1016 1030 1031 1038 1042 6.5 ADC Modules with CMN (micro-discharge problem) Common mode subtracted noise in blue For majority of modules with problems, the common mode subtraction is imperfect. 7 of 12 have >2.0 ADC noise 3 of 12 have >3.0 ADC noise (Two times regular noise)

11 11 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Common Mode Subtraction Variation Common mode subtraction results inconsistent  Answer differs mode-to-mode or test-to-test  Would yield varying signal efficiency/noise during data taking  Not clear how this will evolve with time/radiation Module 1016Module 1010

12 12 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Study of Common Mode The common mode point is calculated event-by-event for groupings of 32 channels  The spectra of the common mode is fit for groupings within a chip with CMN problems Excluding the grouping with high noise channel Spectra is fit with two Gaussians  Central core plus tail  Fit parameters are: Fraction of events in tail Width of central core Width of tail Study how parameters vary with current

13 13 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN Problem Module After Re-Probing Last SS6 module built using one sensor with 1.2  A extra current (450 nA vs 1700 nA) in UCSB re- probing at 450 V.  Well within old selection criteria  No large addition increase in current during module assembly  Old sensors 30210320274206 30210320274214 CMN seen in chip 46 with extremely high noise in channels 423-424  Sensor flaw seen between two channels Not clear if flaw cause of problem  Begins at 400 V where database and measured bias current diverge ~0.5  A difference

14 14 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN Problem Module After Re-Probing Module tested at slightly elevated voltage to measure effect as function of current  Bias current 3.7  A, < 2  A more than expected from database For first half of chip, CM subtracted noise a factor of ~1.75 higher than typical noise.  A very little amount of micro- discharge can cause the CM subtraction algorithm not to work properly CM subtraction algorithm used is same as LT, and test beam software

15 15 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 CMN Problem Module After Re-Probing Micro-discharging strip dis-appears/appears randomly But always with the same 2 IV curves It IS NOT clear if module which is tested today will be good tommorrow

16 16 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Module 705 before LT (FNAL) After assembly module was tested (09/08) on ARCS at 400 V and graded “B” (6 faulty channels). No problems observed.

17 17 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Module 705: LT data (FNAL)  Data was taken at  20°C on Sept.19 (10 days after the first test). A group of high noise channels is seen around channel 219 and increased CMN is seen in chip #2

18 18 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Comparison of IV curves (FNAL)  ”before” measurement is taken on 09/08 on ARCS before LT  “after” measurement is taken on 09/23 on ARCS after LT  green curve is a measurement done using Keithley on 09/24 with 1 minute interval between steps No visual defects are observed on the sensors around noisy channel #219 We know it is not a humidity effect: 3 weeks in dry air did not cure it

19 19 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 “Fix” For CMN Problem Modules In most cases, the CMN can be removed from chip by:  Removing bond from effected sensor  Adding Bond between AC pad (AL strip) and bias ring Uses the coupling capacitor as a high-frequency shunt of the increased current  Thus, neighbors do not see noise  Increases noise on sensor edges due to increased current on bias ring Does not increase (or decrease) current drawn by module The long term stability of this fix is not known  Cannot apply this fix once installed on rods, petals, or in detector

20 20 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 How Does ARCS React to CMN Problem 25 ADC 869 881 1010 1011 1013 1014 1015 1016 1030 1031 1038 1042 6.5 ADC Common mode subtracted noise in blue With standard fault finding, only CMS noise would flag problem Of 15 modules, 7 would be graded A or B Since CMN varies with time and mode, grading varies with time Module’s high current would generally indicate a problem though.

21 21 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 How To Modify Programs To Increase Sensitivity of CMN Add grading due to bias current directly into program Add flag of major problem if noise of any single channel above 20 ADC Add flag of major problem if average raw noise of a chip above 2 ADC (Peak) and 2.5 ADC (Deconvolution) The average raw noise already in output can quantify size of CMN RMS of CMS noise per chip could be used as an indicator of how well the CM subtraction works on module BUT AS A REMINDER, THERE IS NO GUARANTEE THAT THE PROBLEM WILL BE THERE AT THE TIME OF THE FIRST TEST !!!  1 module at UCSB has the problem coming and going randomly  1 module at FNAL developed the problem during LT test

22 22 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Conclusions We are seeing time evolution of the sensors These sensors cause CMN noise on a chip with a turn- on distribution between 50-450 V  The noise is not always subtractable  The noise varies with time significantly  It would be a nightmare to commission/operate a detector of this size with ~5% modules with this effect With pre-probing, the rate of the problem is reduced  BUT NO way to know if the sensors will continue to evolve The current testing protocol will find the problem if it exists at the time of the test  But there are many good reason to believe that many module WILL NOT have the problem at the time of testing, but will develop it later

23 23 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 IV Test Results (UCSB) Environmental conditions tightly controlled  Temperature 23.1-23.8 C  RH < 30% at all times An increase greater than 5  A can cause CMN Much better results with newer OB2 sensors (2002) None of the 20 newest (2003) OB2 sensor show any increase in bias current!!! Sensors> 2  A > 5  A >10  A >20  A >100  A < -2  A <-5  A <-10  A OB2 (’00-01)15%9%8%5%1%8%3%1% OB1 (’00-01)6%3% 0% OB2 (’02)3% 0% 2% 0% OB2 (’03)0% Probed Current @ UCSB (400 V) – QTC Measurement (400 V)

24 24 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Could Grounding Cause The Problem? It is extremely unlikely that grounding could create or enhance the CMN problem LV and HV supplies floating  Same as the final detector Clamshell  Module holding plate in clamshell but isolated > 1cm from metal shell  Grounding achieved with large gauge wire to hybrid-to- utri adaptors Four grounding schemes studied  Grounding clamshell/module carrier Grounding used chosen because it minimizes the CM noise and sensitivity to environment Only changes made relative to standard test stands at time were:  Grounding hybrid-to-utri adaptor to test box instead of module testing plate  Use of a thick, continuous, metal shield Most centers now have use the same grounding scheme

25 25 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Noise vs. Grounding CMN seen in both ARCS LT  Answer differs mode-to-mode, test-to-test, test stand-to-test stand Grounding vastly different  ARCS use floating power supplies and “star” grounding Only one common point  LT have non-floating power supplies and everything is grounded to everything else Multiple ground loop Module 1016 (ARCS)Module 1016 (LT) Raw NoiseCMS Noise

26 26 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Why isn’t problem seen at test beam? Most of modules pre-screened against the CMN problem prior to shipment to CERN  All of UCSB modules sent either do not have problem or have had enough channels pulled in order to remove problem  Most of FNAL modules sent after they began pre-screening for problem Only 6 modules made with flex hybrids sent without testing at 400 V ~50% of the time, 0 of 6 modules would not have this problem Assumes that the rate of problem and distribution of CMN turn-on voltage constant We know that many sensor effects are severely batch dependent Many possible reasons why not seen in old prototype modules  Many circuits in prototype ceramic hybrids have been changed  Testing methods have changed  Maybe batch of sensors used in production did not have the problem Well, it was in test beam. 2 with turn-on voltage of 400 V  See L. Borrello’s talk in sensor meeting

27 27 CMN Problem Review-Anthony AffolderTPO, December 11, 2003 Fit Result of Common Mode Point Fraction of events is flat with bias current (~strip current) Width of central core increases with bias current (~strip current) Width of tail increases with bias current (~strip current) and may flattens out at some current


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