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25.2.04TRD Collaboration meeting GSIClemens Adler First Production Chambers Production/tests/results
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25.2.04TRD Collaboration meeting GSIClemens Adler Production of first Chambers Nov/Dec: Vist from Oleg and Sasha (Dubna): Parallel production of 2 chambers at Heidelberg Test of chambers: Christmas 2003- January 2004 New(s) (Challenges): -Glueing of Padplane-panel- assembly (100 cables have to be fed trough holes) -Wacosit Profile extruded in final shape (easier to use than standard G10 parts) -Winding machine after modifications
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25.2.04TRD Collaboration meeting GSIClemens Adler Padplane glueing Feeding cables trough Backpanel cutouts worked well Glueing of Padplane to Honeycomb works, but can still be improved
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25.2.04TRD Collaboration meeting GSIClemens Adler Wacosit profiles Wacosit is behaving good, minor quality improvements are discussed with Manufacturer
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25.2.04TRD Collaboration meeting GSIClemens Adler Wiring Oleg glueing Anode wires
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25.2.04TRD Collaboration meeting GSIClemens Adler What we learned: All current materials behave well. Tooling needed: –Positioning of wire ledges, –Distance ledges –Crane for lifting of winding frame (installed in January) –New winding frames (arrived)
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25.2.04TRD Collaboration meeting GSIClemens Adler Tests Dark current: (Was a Problem with Prototype chambers) At first dark current started at ~1400-1500V. After some conditioning (over night at <50 nA) Dark Currents <1 nA Leak Rate Gain uniformity
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25.2.04TRD Collaboration meeting GSIClemens Adler Preparation for tests Grounding of Padplane: –Adhesive copper tape: not reliable –Foldback clips, w. conductive foam: Complicated to use ->use of PCB with real connectors to ensure reliable grounding of Padpane while testing (in devel.) Gas filling: Issue: time Procedure: flush Chamber with 80-100 l/h Ar/CO2 with open Gas-in-outlets. 1000 ppm O2 level after 2-3 h. Connect outlet etc. and flush at 20 l/h overnight ->few ppm level next morning
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25.2.04TRD Collaboration meeting GSIClemens Adler Leak rate Determined by measureing O2 concentration (and assuming diffusion leaks) Upper limit: 1,5-3 mbar*l/h Test chamber performance: <0,5 mbar*l/h Problem: very large leaks (some l/h) will also show „reasonable“ leak rates (<3mbar*l/h) with O2 method. Solution: –Check that gas exits chamber down to low flow rates (1 l/h) –Use sniffer to detect leaks
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25.2.04TRD Collaboration meeting GSIClemens Adler Leak rate cont. Leakage of two connected chambers: Sniffer could detect leaks at gas connections. ->grease should be used to improve leak rate
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25.2.04TRD Collaboration meeting GSIClemens Adler Gain Uniformity Chamber1 Left: copper tape grounding Below: foldback clips
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