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New Richmond Load Serving Study Northern MAPP Subregional Planning Group August 16, 2006 Daniel Kline
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3 Outline Description of Area Various Load Serving Problems Study Methodology & Initial Alternatives Final Alternatives Considered Final Recommendation & Initial Project Schedule Questions
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4 Description of Area Located in Western Wisconsin St. Croix County Just across Minnesota border, near I-94 Area fed by 161 kV sources and 69 kV subtransmission Load belonging to Xcel and DPC Lines belonging to Xcel and DPC
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5 Description of Area Area Xcel Loads (2011): New Richmond (9.1 MW) Somerset (7.7 MW) Kinnickinnic (4.4 MW) Osceola (15.4 MW) River Falls (30 MW) Area DPC Loads (2011): New Richmond (15 MW) Houlton (5.4 MW) Farmington (8.1 MW) Roberts (4.6 MW) Hammond (3.2 MW)
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6 Description of Area
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7 Description of Problems Low voltage at New Richmond during outage of Pine Lake – New Richmond 69 kV line Low voltage at Osceola during outage of Osceola – Osceola Tap 69 kV line Overload of River Falls 115/69 kV transformer during outage of Osceola – Osceola Tap 69 kV line Overload of Pine Lake 161/115 kV transformer during outage of King – Willow River 115 kV line Normal Overload of Pine Lake – Rush River 69 kV line
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8 Description of Problems High load growth throughout area Installation of Chisago Line Project will require extended outage of Osceola – Osceola Tap 69 kV line No room for expansion at New Richmond Substation No room for expansion at Rush River Substation
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9 Study Methodology 2006 MAPP Series Cases 2011 Near-Term 2016 Out-Year Study Group Asked to Review: Jerry Iverson, DPC Bob Roddy, DPC Dave Krause, KPE Jeff Haas, Xcel Walt Grivna, Xcel
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10 Study Methodology Assumptions and Adjustments made Assumed Chisago Line Project not in service in 2011 (In-service in 2016) New City of New Richmond Substation in service Xcel’s Somerset Substation in service Added DPC N-60 line upgrade (477 ACSR)
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11 Study Methodology Base Case Results
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12 Study Methodology Base Case Results
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13 Initial Ideas Multi-Faceted Approach 5.4 MVAR Capacitor at Osceola 10.0 MVAR Capacitor at New Richmond New 69 kV switching station south of New Richmond that would tap DPC N-60 line 115/69 kV Transformer near Kinnickinnic Substation 161/69 kV Transformer at Clear Lake Substation 69 kV line from Somerset to new substation north of New Richmond 69 kV line from Cylon to new substation north of New Richmond
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14 Initial Ideas Options investigated with and without Chisago project Necessity of Poplar Lake Substation and 161/69 kV transformer investigated
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15 Final Alternatives Three options tagged for detailed review Alternative 1, Step 2A – Three Lakes 115/69 kV Substation, Stanton 69 kV Substation, & Somerset to Stanton 69 kV Line Alternative 1, Step 2B – Three Lakes 115/69 kV Substation, Stanton 69 kV Substation, & Cylon to Stanton 69 kV Line Alternative 2, Step 1 – 115/69 kV Substation south of New Richmond
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16 Final Alternatives - 1
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17 Final Alternatives - 1
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18 Final Alternatives - 2
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19 Final Alternatives - 2
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20 Final Alternatives - 3
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21 Final Alternatives - 3 Voltage Violations too numerous to mention
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22 Final Recommendation Alternative 1 Recommended 10 MVAR Cap Bank at New Richmond – ASAP Three Lakes Substation – ASAP 5.4 MVAR Cap Bank at Osceola – May 31, 2009 Rebuild Osceola to Sand Lake 69 kV Line – May 31, 2009 Relocate Rush River Substation and cut over to 161 kV – May 31, 2010 Construct Somerset Sub – May 31, 2010 Construct Stanton Sub – December 31, 2010 Construct Somerset to Stanton 69 kV Line – May 31, 2011 Complete installation of Chisago Line Project – May 31, 2011 Construct Poplar Lake Sub & 161/69 kV Transformer – May 31, 2011
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23 Next Steps Currently compiling necessary information for business case Will have more meetings with Study Group prior to any filings
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