Download presentation
Presentation is loading. Please wait.
Published byKelley Rodgers Modified over 9 years ago
1
DC Motor Control Project Group A ALEXANDER M FUNK LAM D NGUYEN JAKEISHA D THOMPSON PAULETTE J VERNON ERIC G ZAISER 12/03/01
2
Introduction Motor Design Motor Construction Problems Control Design Control Problems Final Results Conclusion
3
Project Overview Design, construct, and control a dc homemade motor, commutation system, control system, and a speed measurement device such that the machine assembly rotates at selected speeds Create a detailed web-page to outline the development process
4
Specifications The outer diameter of the rotor: 1.5 and 4.5 inches. The length of the rotor housing: 2 and 6 inches. A commutator must be built. Standard magnets must be used Supply jacks must be supplied for an unknown resistance
5
Schedule
6
Motor Design Four Pole Motor Simplex Lap Winding 45 windings 26 gauge Copper Wire Steel Stator – 3.5“ inner diameter and 4” outer diameter 16 magnets(1” by ½“ by ¼“) acting as 4 poles JB Weld to place magnets Steel rotor-2” diameter 25 1/8” thick, 2.5” outer diameter discs; 12-0.35” diameter holes
7
Motor Design 4 brushes alternating at 90° 3/8” Shaft Polyurethane lamination
8
DC Permanent Magnet Motor
9
4 Pole Simplex Lap Winding
10
1.5 inch inner diameter copper pipe 12 segments required for four pole operation Vinyl insulation from the shaft Brush contact 12 segments (2 x 0.78 inches ) Epoxy to fill in slots Commutator
11
Motor Construction Problems Uneven commutator bars Drilling through copper for hooks Commutator bars popping off Misalignment of magnets in the stator Fitting the bearings onto the shaft Sliding of shaft as motor was spinning Friction in commutator from lack of epoxy
12
The Final Product
13
Control Basic Hardware Setup Initial Research Regarding Motors Limited Theoretical Modeling “Control Theory” group shifted to “Test & Fix” Group
14
Control Implementation Encoder Open Loop/Bonus day PID implementation Tweaking/Tuning Competition
15
Control System in Simulink
16
Control Problems Encoder-related Mounting Cable Motor-related Friction Drift/alignment Simulink-related Disappearing feedback
17
Final Results Bonus Day :300 rpm 10 points Competition Day: 1 st Place Average Steady State Error of +/- 5.33 RPM Transient score of.4165
18
Transient Response
19
Conclusion Motor design was outstanding Steady state control was outstanding Control system was outstanding Group A is Great!!
Similar presentations
© 2025 SlidePlayer.com. Inc.
All rights reserved.