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nEDM Collaboration Meeting, November 1-3, 2007 Valve Progress Steve Williamson, UIUC
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nEDM Collaboration Meeting, November 1-3, 2007 Bucket Dewar Tests Testing of the Vespel “cork-in-bottle” seat was successfully completed. 1” diameter, 80 lbs closing force 10750 continuous cycles Leak rate < 3 10 -8 std. cc/sec (background rate) with super-fluid He at 1.7 K … But not without some difficulty
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nEDM Collaboration Meeting, November 1-3, 2007 Testing Problems Accidental warm-up caused leak at “press-fit” inlet connection shortly after the Annual Review. May also have caused cold leak in Vespel (or could have been caused by new flange connection) Re-fabricated seat and plug had bad surface due to chipped diamond tool. Re-re-fabricated plug was slightly off-axis. Actuator motion was impaired by lack of lubrication. Actuator controller died due to leaky capacitor – paused final cycle test for about a day About a month of frustration Stick-slip from non- concentric plug Sticking in actuator
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nEDM Collaboration Meeting, November 1-3, 2007 Postmortem after 10,000 cycles Visual inspection: no obvious signs of wear except a light ring at seal line.
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nEDM Collaboration Meeting, November 1-3, 2007 Diamond machined surface Region where surface has been scraped during closure Vespel builds up in a ridge above the seal line SEM Scans* of “Piston” SEM scan of seal line after a few hundred cycles SEM scan of seal line after >10000 cycles Note: This is NOT the same “piston” Diamond machined surface seems smoother Ridge (Vespel build- up) at seal line is narrower. * Thanks to Steve Clayton!
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nEDM Collaboration Meeting, November 1-3, 2007 Another SEM Picture of Seal Line after 10,000 cycles Ridge seems pretty sharp. Dust particles (below line) – easy targets for focusing.
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nEDM Collaboration Meeting, November 1-3, 2007 Another SEM Picture of Seat after 10,000 cycles Below seal line, edge is rough – accumulated dirt? Focusing is not easy. Beveled seat edge Seal edge
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nEDM Collaboration Meeting, November 1-3, 2007 Plans for Bucket Dewar Testing Try to eliminate “popping” of the cork (may or may not be an improvement). Does not happens if tan( ) > is the static coefficient of friction. For 300K Vespel, 0.35, so must be > 19°. At lower temperature, may be smaller. Our valve had =10°. “Cork Popping” Position Load
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nEDM Collaboration Meeting, November 1-3, 2007 Try to reduce closing force. Engineers: How Much? Scaling the valve to 3.5 cm diameter implies closing force of 110 lbs. Everything is easier for lower closing force Mechanical support of valve can be less massive (lower heat load) System for transmitting force can be less massive (lower heat load) Valve wear should be reduced Try materials softer than Vespel Kel-F Acrylic Plans for Bucket Dewar Testing Rockwell Method
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nEDM Collaboration Meeting, November 1-3, 2007 K. D. May, “Advanced Valve Technology”, NASA SP-5019, 1965 Soft close-fitting tip could act as “wiper” rather than “scraper”. Plans for Bucket Dewar Testing Try adjusting seat geometry May contribute to lowering seating force May improve immunity to dirt Some Ideas: NASA “Scrubber” design Soft (Kel-F?) wiper on plug
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nEDM Collaboration Meeting, November 1-3, 2007 Highest Priority: Full Valve Test Goals: Fabricate a full-sized valve Use reasonable (though not necessarily final) materials Test it under realistic conditions LHe II inside at ~1.7 K Vacuum outside Hardware required: Large (12” ID) dewar Dewar insert with 1 K pot, motion feed-thru, and gas/vacuum/instrumentation lines A valve
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nEDM Collaboration Meeting, November 1-3, 2007 The Dewar Ordered from Precision Cryogenic Systems $8.1K Delivery: 3-4 mo. (~Jan ’08) Features Super-insulated (no LN 2 shield) ~50 l “belly” Matched in dimensions to insert
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nEDM Collaboration Meeting, November 1-3, 2007 The Insert Ordered from Janis $27.3k Delivery: 3-4 mo. (~Jan ’08) Features: 100 mW cooling power at 2K LHe throttle valve on 1K pot 6 ½” lines (1 removable) Two motion feed-thru lines Large internal vacuum volume
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nEDM Collaboration Meeting, November 1-3, 2007 The Valve Design by Bartoszek Eng. based on Jan’s earlier concept Double seal (open and closed) using our best design. Open seal hides bellows from 3 He. Be-Cu bellows assembly (from Mini-flex) All Be-Cu welding to be performed by vendor Design of assembly has iterated with vendor Acrylic body Current plan is to cast, then final machine. A glued prototype is being fabricated. Open Seat Closed Seat Plug Bellows Assembly Acrylic Body Inlet Outlet
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nEDM Collaboration Meeting, November 1-3, 2007 Valve Issues Bellows assembly may have long lead time (no estimate yet) Cast acrylic body may have long lead time. Fall-back: glue the assembly. Actuator must be modified: controlled force required when closing and opening. Delay in dewar and insert We will do plenty of room temp tests (dewar and insert may not actually be on critical path). Fall-back: do bucket dewar tests in 3 He refrig. cryostat. This conflicts with polarized 3 He lifetime studies.
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